


Mileage: a lot
Repair History: Dave®
-- Dave Foster wrote:
>
> Hi all I got a 1989 full size chevy pu trk 2x4 that I rebuilt the trans
> in 700-R4 . the unit works great , but while driving down the road at a
> steady speed the converter will unlock & lock back up for no reason.
> the scanner shows it lock & unlock and you can feel it ,But it stays in
> closed loop. The unit has new solenoid ,pressure switch & temp switch in
> the trans , and sets no codes.
> also the brake light switch has been replaced , because sometimes the
> cruse control just shuts off & unlocks the converter , and the dealer
> said that they have had a lot of trouble with this switch . well the
> unit still locks & unlocks & the cruse will still just shuts off at
> random , the truck stays in closed loop.And the thermostat has been
> changed , the tps has been tested unable to find any glitches in it so
> far . the map sensor vacuum lines are in good shape . but this thing
> still unlocks and locks back up while driving steady and the cruse still
> just shuts off randomly.
> the speed sensor seems to work just fine.
> doe's any one have any ideas for me on what to do or check next ? Thanks
> for your help in this matter.
>
> Dave Foster d.b.a. The Transmission Technician
> 1312 Morningside Dr Melbourne Fl 32901
> transtech@metrolink.net
> AAMCO master certified-ASE-ATRA
> Proud member of TRNi-technicians from around the world
> working together on today's sophisticated transmissions
> TRNi is second to none
Dave Foster The Transmission Technician
transtech@metrolink.net phone / fax (407)728-1155
Home page
Work Completed: Everything everyone posted
Summary: Sorry it took four months to Re:
I can't work on it going down I95
David Foster
transtech@metrolink.net
David Foster
transtech@metrolink.net
Roger Pryor
whizwheel@aol.com
David Foster
transtech@metrolink.net
Leonard Marucci
len@kwiknet.net
Jean Bracconier
trantech@ilos.net
Ted Turney
tedeb@prodigy.net
Daniel Wills
dwills@foxinternet.net
Steve Allbee
steve@customtrans.com
Jeff Anglesey
oldtimer57@hotmail.com
Mike Sullivan
advance@cowtown.net
David Foster
transtech@metrolink.net
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Mileage: N/A
Repair History: Hi Joe, It would be a lot easer to respond, if the post was done as a new problem. Instead of : Problem/Fix. Once the Fix is in the subject. The thread on the web site is closed. I think that you will have better luck getting help if you just post it as a new problem. ( JMHO )
Work Completed: None
Summary: Hi Joe,
in 1985 GM. added a dam neer thr pump bolt hole buy the pressure blow off ball and spring.
The area between the dam & bolt hole is now a void. cross leaks may fill this void with
oil so an orficed cup plug was removed to give the void full exhaust.
When an early pump body, no dam, is matched with a late cover then line pressure goes past
the dam and out the exhaust hole. This causes low line pressure,delayed engagements, and
slipping on shifts.
Forget the casting numbers!
Late pump covers will fit all pump bodies if you modify them buy pluging the exhaust hole.
Use the small orificed cup plug avabile in SK 700 & SK 22-79 Shift kits.
Early pump covers will fit all pump bodies as is.
Late pump bodies will fit all pump covers as is.
Early pump bodies will fit early covers as is & modified late covers.
Summary: Always plug the hole in the late cover, then mix & match bodies and covers any
way you choose. All of this info is in the A.T.R.A. 1990 seminar manual.
David Foster
transtech@metrolink.net
David Foster
transtech@metrolink.net
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Mileage: 120915
Repair History: Hi Group, I am having a problem with the speedo driven gear on the truck. It rounds out the square drive part of the Driven gear. It has the 90 adapter that goes on the speedo bullet which has been replaced also.
Work Completed: If I take the bullet attach it to the adapter and install a driven gear into it I can turn the gear by hand and it is free and smooth.This has stripped out the driven gear 3 times now in less than 200 miles. And there is no signs of any other gear damage ( hour glassing ) On the third try I even super glued in the drive lug into the driven gear, so I knew that the drive lug was getting full contact into the driven gear, for the most support. Do you have any idea as to what is causing this?
Summary: Need Help
does anyone make a steel shank gear like chrysler for GM
Thanks!
David Foster
transtech@metrolink.net
Rod Cayko
cayko@aol.com
David Foster
transtech@metrolink.net
Chuck Clampitt
mrshift@starcomm.net
David Foster
transtech@metrolink.net
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Mileage: 97762
Repair History: none that I know of
Work Completed: Rebuild with reaction planet and all the goodies
Summary: Hi Group,
It's dumb question time again. I have a aluminum drive shaft in this truck
and when I went to pull it I had to pry it out of the companion flange,
when I got it out I have 2 coil tapered springs inside of the yoke.
They load the output shaft to the front of the transmission. I have
never seen anything like this before ( so im a little slow ) Are these
springs suppose to be in the yoke and if so why. Are they to deaden noise
or something? I just do not see why they would want to load the
output shaft.
These springs look like the ones that they use on the exhaust
manifold only they are shorter and heavier.
Has anyone else ran into these springs? And are you replacing them?
Thanks!
David Foster
transtech@metrolink.net
Jim III
stardust@frontiernet.net
Cliff Westendorp
cwestendorp@msn.com
David Foster
transtech@metrolink.net
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Problem/Fix: How many of you use flat washers between flex plate and TC? How many have actually measured a batch of 'typical' 3/8" flat washers for thickness? I've been checking them before use, I find them from 0.060 all the way to 0.082......which makes me wonder if maybe some converter run-out problems are from this source. If anyone wants to discuss it further, I guess we won't get thwacked TOO hard if we take it to -2.
Gary Glaenzer
debngary@irtc.net
Mileage: 105,000
Repair History: overhaul on 9-11-99
Work Completed: removed and disassemble
Summary: hello all i built this unit on 9-11-99 and came in today with 1st
gear only. removed and desassembled found the band burn't and also
3-4 clutches. looks like it took some time to burn them up. any ideas
the rest of the trans looks good. has about 3000 miles since i did
the trans thanks terry..........
Terry Neuendorf
qualitytrans@earthlink.net
Jim III
stardust@frontiernet.net
Donald Stone
aaatrans@treco.net
Larry Bloodworth
larry_b@certifiedtrans.com
Roger Pryor
whizwheel@aol.com
Leo Schneggenburger
transfixleo@netscape.net
Richard Randleas
rrandlea@gwtc.net
Joey Campbell
bccampbe@neocom.net
Glenn Morse
tranny1@aol.com
Terry Neuendorf
qualitytrans@earthlink.net
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Mileage: 80k
Repair History: none by me, someone had overhauled it before, but cooler was plugged solid.
Work Completed: works good, used big Tru-Cool instead of radiator cooler
Summary: Just wondering about overfilling 700's.
Can't recall ever seeing the subject discussed.
Anyone have any thoughts?
Gary Glaenzer
debngary@irtc.net
David Foster
transtech@metrolink.net
Jim III
stardust@frontiernet.net
Roger Pryor
whizwheel@aol.com
Gary Glaenzer
debngary@irtc.net
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Mileage: 80k
Repair History: none by me
Work Completed: decided to seek info before tackling this one
Summary: This truck has a 3" suspension lift.
Owner states that he has put 4 sets of dront axles in it in 15 months...they either 'pop' out of the retainer, or pull the CV joints apart.
Any cure, except to take out the lift?
BTW, the 'lift job' was kind of done 'half-way'......lower arms were not replaced, just the uppers.
Gary Glaenzer
debngary@irtc.net
Fernando Rosales
surflobstr@aol.com
Dale Snyder
dalesnip@cs.com
Gary Glaenzer
debngary@irtc.net
Gary Glaenzer
debngary@irtc.net
Gary Glaenzer
debngary@irtc.net
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Mileage: 108K
Repair History: N/A
Work Completed: Tear Down
Summary: Question. This vehicle has oversized tires and 4" lift kit.
Input planet destroyed and ring gear split in two places.
My question is what causes this. I have not seen it happen in years. Am I dealing with abuse or what. Thanks, Jim, III
Jim III
stardust@frontiernet.net
Paul Moore
n8249b@aol.com
Steve Allbee
steve@customtrans.com
Jim III
stardust@frontiernet.net
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Mileage:
Repair History: Rebuildt trans.
Work Completed: Cannot get power to Trans. electrical conn. Cked. wires, fuses, brake switches, new lock up relay under dash.
Summary: Need wire diagram showing lock up system, seems like the lock up relay is not getting grounded. Where to from here?
Leo Weber
alextran@rea-alp.com
CJ of-Canada
info@transtechca.com
Leo Weber
alextran@rea-alp.com
Robert Bruce
robertlb@ev1.net
Joey Campbell
bccampbe@neocom.net
Harold Field
trblshtr@tdstelme.net
Robert Bruce
robertlb@ev1.net
Donald Stone
aaatrans@treco.net
Dan Tucker
transman@prodigy.net
Larry Bloodworth
larry_b@certifiedtrans.com
Roger Pryor
whizwheel@aol.com
Roger Pryor
whizwheel@aol.com
Joey Campbell
bccampbe@neocom.net
Leo Weber
alextran@rea-alp.com
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Mileage: mega
Repair History: none
Work Completed: none
Summary: customer wants to install a 700 Iam looking for a shaft that is shorter so his existing t-case will bolt up direct. I have cut and welded these before. just looking for a better deal. need a supplier.
Jeff Anglesey
oldtimer57@hotmail.com
Jimmy Taylor
odie@gci.net
Richard Smith
mrtrans@worldnet.att.net
Jeff Anglesey
oldtimer57@hotmail.com
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Mileage: 000
Repair History: install engine and rebuilt trans
Work Completed: none
Summary: I hope this thing hasn't gone in about 5 times, I am having quite a time to day. Any way to speak of this trans problem. no 4-2 or 3-2 after about 40mph. it will make a 4-3. this trans has a transco shift kit and a new s plate. has new pressure reg valve .500 tv boost valve. Iam thinking of stiffing up the tv valve spring. what about the tv limit valve? can some body help
Jeff Anglesey
oldtimer57@hotmail.com
Kit Lindsay
lindsay2@sprintmail.com
John Lovell
ent@crosslink.net
Leo Schneggenburger
transfixleo@netscape.net
Jeff Anglesey
oldtimer57@hotmail.com
Darwin Upton
darwank@usinternet.com
Frank Choate
jfranklinc@aol.com
Larry Bloodworth
larry_b@certifiedtrans.com
Mike Quigley
mikeq@netcom.ca
Jimmy Taylor
odie@gci.net
Jeff Anglesey
oldtimer57@hotmail.com
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Problem/Fix: Here is the GM part # for the 3/8" cup plug that we use in the 2nd servo in place of the check ball capsule. For some reason our parts suppliers can never find it 8620318 Jim, III
Jim III
stardust@frontiernet.net
Mileage: a lot
Repair History: other home worker "overhault" it about 1 year ago (has really unsatisfactory feeling, slipping, binding and all the other great feelings) first loss 3rd and 4th then come in for no move
Work Completed: found some mistakes of the home worker not related to this problem found broken rotor and slide and missing rotor guide pressure relief free to move TV boost ,391"
Summary: What can create the force to broken the rotor in 4 pieces and guide in two?
Is it possible if the pump halfs are over torqued so the slide stucks?
Thanks a lot in advance for all thinkings!
Rosi germany
Falk Rossberg
falkrossberg@t-online.de
Falk Rossberg
falkrossberg@t-online.de
Daniel Wills
danwills@mindspring.com
Falk Rossberg
falkrossberg@t-online.de
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Problem/Fix: Hi group! In a lot of 700 I installed the 3-4commercial pack with good results. TCS recommend for me to use high capacity friction plates for this clutch pack. They tell that many rebuilder prefer it as a equal or better and cheaper 3-4 fix. What is your experience with this stuff? Thanks in advance to all. Rosi germany
Falk Rossberg
falkrossberg@t-online.de
Mileage: lots
Repair History: This unit was installed a year ago by another shop, customer was told it was a 'GM rebuilt'.
Work Completed: Replaced with stock unit, vehicle is gone
Summary: OK.....I was dismantling this unit to rebuild for stock.
Model stamp 9YL088 (??????)
Other curiosities found during tear down:
1) three orificed cup plugs in (a) lo-rev piston feed; (b) governor return; (c) rear hole in 3/4 accum bore
2) small (light-weight) orange spring between servo cover and 4th piston
3) Check ball (5/16) in solenoid snout
4)It appears to have a transgo kit in the T.V. bore, can see the tiny spring at end of plunger.
5) trans-tec gaskets
6) unit has 'Type 5' wiring, which was wrong for the vehicle, but internal harness plug was unhooked.
7) early style input sprag.
8) no aux VB
9) small 'tit' of casting in the TV exhaust ball space (assume to prevent accidental installation of a ball there)
I've already made the decision to scrap this case and VB (don't care to unravel puzzles )but just curious as to what brand shift kit may have used these mods.
Or was this a 'factory reman', with the orificed plugs (but why are they in there???)
The date-code stamp is identical in size and letter shape to a factory one, and there are remains of the original underneath (but not readable).
Gary Glaenzer
debngary@irtc.net
Don Oremus
dkoremus@execpc.com
Gary Glaenzer
debngary@irtc.net
Robert Bruce
robertlb@ev1.net
Don Oremus
dkoremus@execpc.com
Falk Rossberg
falkrossberg@t-online.de
Gary Glaenzer
debngary@irtc.net
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Mileage: 230000KM
Repair History: none
Work Completed: only first & sec. gear / no engine braking
Summary: Is ther a particular reson for the hub to break abart from driver
abuse.
Theo from downunder
Theo Heindl
theobald@ozemail.com.au
Jimmy Taylor
odie@gci.net
Joey Campbell
bccampbe@neocom.net
Theo Heindl
theobald@ozemail.com.au
Fernando Rosales
surflobstr@aol.com
Jim Eberhart
eberhart@efortress.com
Roger Pryor
whizwheel@aol.com
Theo Heindl
theobald@ozemail.com.au
John Tate
autots@tpgi.com.au
Theo Heindl
theobald@ozemail.com.au
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Mileage: 20,000 km
Repair History: Customer (another shop) installed this 4cyl Perkins diesel & 700 trans, unit came in first time with improper TV arm ratio setup & trans smoked. Begged us to help him (my first mistake) we rebuilt trans & tv problem was corrected. All was well for 2ooo km & lost lockup.... fluid smelled. Pulled trans & clutches all ok, but TCC is burn't, repalced pump & installed lo stall torque & all was well again for 1500 km & guess what no TCC operation. I am not taking any responsibility for this mismatched set up, now he wants me to build it with no lockup. I have info from Steve Younger seminar years back on building "de-lock" 7oo unit. My question is has anyone done this & does it work ??. This engine is about 120 HP only rev's to 2400 rpm but has a very low power band, final drive is 3:73 ratio.
Work Completed: None
Summary: Will this setup work or are we setting ourselves up again, he had prevous vehicle basically same setup with 350 trans & drove it for 2 years but top speed was 80 km (50 mph).
Ken Buehler
kbuehler@freespace.net
Donald Stone
aaatrans@treco.net
Larry Bloodworth
larry_b@certifiedtrans.com
Leo Schneggenburger
transfixleo@netscape.net
Greg Boehm
greg@valtran.com
Donald Stone
aaatrans@treco.net
Daniel Wills
danwills@mindspring.com
Ken Buehler
kbuehler@freespace.net
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Problem/Fix: 77 CHEV Change over TH 350 to 700R4. The 700r4 that will be installed has a one wire lock up system. 1. Is there such a item as wiring torque converter lock up kit that can be installed, when making this kind of change over? 2. And Can someone tell me what to do or where I can get a wiring diagram? Thanks Walt
Walt's Trans
waltg@relia.net
Mileage: new motor
Repair History: pulled unit complete rebuild, fades in and out of lock up on slightest incline.
Work Completed: pulled valve body, changed lockup spring, still does same thing. Also hydralickly locked. same thing. All electrical put back in and worked for a week, now i am back to square one.
Summary: has anyone ever had this problem and know of a fix? Please help having hard time with this one. Thanks, Justin jmpjdp@nque.com
Justin Painter
jmpjdp@nque.com
Kim Walton
citytrans@webscene.com.au
Falk Rossberg
falkrossberg@t-online.de
Justin Painter
jmpjdp@nque.com
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Mileage: 331,000
Repair History: rebuilt about 2500 miles back all upshifts are good and at the right time
Work Completed: coming back wed.
Summary: around 70 -80 mph if you accelerate fairly hard it will shift back and forth between 4th and 3rd. It will keep doing this until you let off or kick it all the way down. Has anyone run into this before? Thanks Archie
Arch Haymaker
archie@ionet.net
Donald Stone
aaatrans@treco.net
Roger Pryor
whizwheel@aol.com
Jim Eberhart
eberhart@efortress.com
Kit Lindsay
lindsay2@sprintmail.com
Kit Lindsay
lindsay2@sprintmail.com
Arch Haymaker
archie@ionet.net
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Mileage: 150,000
Repair History: Rebuilt about a year ago. Normal rebuild.
Work Completed: Came back with the inner low/rev sprag race broke, rear carrier broke, metal, etc. Rebuilt, pressure tested, new pump, converter, etc. Has a delay in rev.
Summary: We have a 1988 full size Chevy with a 4l60 (700-R4). Came in (came back rather) with the rev sprag, rear carrier, etc. broke. We rebuilt it. After we rebuilt it there was a slight delay in rev and when you accelerated rapidly, it would bang in. Like maybe one unit is not applying at first. We seem to have no rev boost at idle. At 1000 RPM pressures are normal. Min and max TV pressures good. It's just at idle that we do not have any rev boost. We have replaced the pump with one that has a .030" larger TV boost valve and a .010" larger rev boost valve. Pump rotor to face clearance is about .002" versus .005" in the old pump. New pump even has an inner pump spring where the old one didn't. We thought all this would fix it but nooo. We just don't have any boost at idle. At 1000 RPM all is ok. Idle speed is 500 in drive. Is that normal? Any ideas?
Thanks,
Dell Wellons
woodchpr@worldnet.att.net
Leo Schneggenburger
lschneg1@rochester.rr.com
David Foster
transtech@metrolink.net
Dell Wellons
woodchpr@worldnet.att.net
Donald Day
trnsmaster@home.com
Robert Bruce
robertlb@ev1.net
Leo Schneggenburger
lschneg1@rochester.rr.com
David Foster
transtech@metrolink.net
Ron Geddert
dadstran@home.com
Dell Wellons
woodchpr@worldnet.att.net
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Mileage: ?
Repair History: Overhaul in progres
Work Completed: n/a
Summary: I have ATSG manual, they recommend reducing size of bleed orifice in piston, they say with "Techpack" p/n 77761c. I can't get one of these here in Denmark !! But what size is the orifice after modification ?? I will plug it and then drill !!
Bent Pedersen
blp@post7.tele.dk
Gary Glaenzer
debngary@irtc.net
Bent Pedersen
blp@post7.tele.dk
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Problem/Fix: Awhile back there was questions about the size of the orifice plug. For years I have been using delco #86311146 & nothing else just install & forget it.
Jeff Balak
kdhtrans55@aol.com
Mileage: unknown
Repair History: Hi group! The car was factory equipped with the 700R4. Someone have taken a swap to 400. Looks like professional job.
Work Completed: The 400 is now worn out and the customer wants to get the original tranny. To do this I have a 700 in stock. Came out a 305" from ´87. plate AA, auxl.body, last steel reverse input piston
Summary: What changes in tranny and also in car must be taken
to make the swap also a professional job.
(Will install TransGo syskocal kit, alto 3-4 commercial,
band kevlar)
Any suggestion would be nice.
Thanks and best regards
Rosi germany
Falk Rossberg
falkrossberg@t-online.de
John Lovell
ent@crosslink.net
Dan Tucker
transman@prodigy.net
Dan Tucker
transman@prodigy.net
Leo Schneggenburger
transfixleo@netscape.net
Falk Rossberg
falkrossberg@t-online.de
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Mileage: 80000
Repair History: none, at another shop that I do plenty of work for.
Work Completed: replaced shift cable, frayed. disconnect wiring and drives fine. turn off cruise control and converter works fine. as soon as you turn the cruise on the converter goes in and out until you let up on throttle or take out the cruise, will do this at any speed, seems to do it worse at higher speed. Does have a code for EGR.
Summary: could this be a ground problem? Faulty cruise.
Steve Allbee
steve@customtrans.com
David Foster
transtech@metrolink.net
Steve Allbee
steve@customtrans.com
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Mileage: unknown
Repair History: 2 yrs on rebuild
Work Completed: tore down for inspection due to metalic fluid,would make a nice paint color.
Summary: Was wondering what causes the sun shell and rev drum tabs to spread apart scraping case. Any Ideas? Thanks Joe
Joe Zahn
rjzahn@usaor.net
Larry Bloodworth
larry_b@certifiedtrans.com
Jimmy Taylor
odie@gci.net
Jim III
stardust@frontiernet.net
Roger Pryor
whizwheel@aol.com
Joey Campbell
bccampbe@neocom.net
Barrie Bowlin
bowlinauto@webtv.net
Joe Zahn
rjzahn@usaor.net
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Mileage: lots
Repair History: rebuilt 6yrs ago, burned 3-4s
Work Completed: fresh overhaul
Summary: Fix data base talks about new throttle valves and sleeves curing this concern, any ideas or fixes? thank you ..Joe
Joe Zahn
rjzahn@usaor.net
Leo Schneggenburger
transfixleo@netscape.net
Roger Pryor
whizwheel@aol.com
Timothy Carney
timjames@prodigy.net
Harold Field
trblshtr@tdstelme.net
Steve Allbee
steve@customtrans.com
Richard Randleas
rrandlea@gwtc.net
CJ of-Canada
info@transtechca.com
Jimmy Newman
cttranny@aol.com
Joe Zahn
rjzahn@usaor.net
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Mileage: 100,000 plus
Repair History: n/a
Work Completed: rebuilding unit
Summary: I'm trying to install the hi-energy 3-4 clutch pack into the input drum. Evidently there is some difference between the 700's and the 4L60E'S, because I can't get the stackup right. I know that the steels are .106 thick, but I can't tell where the difference is. Any ideas? Thanks in advance, Elliot
Elliot Walters
trnsmsn@aol.com
Leo Schneggenburger
lschneg1@rochester.rr.com
Dale Blake
dblake@telusplanet.net
Elliot Walters
trnsmsn@aol.com
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Mileage: N\A
Repair History: N/A
Work Completed: N/A
Summary: I am in search of a reliable way to identify the cases. My employer has some gutted out cases, both 86 types, that may ,or may not, require auxiliary valve bodies. The Feed Back database was inconclusive. Any hints? TIA!
Randy Kanary
kanarys@zbzoom.net
Dale Blake
dblake@telusplanet.net
Chuck Reavis
quui@aol.com
Clayton Allen
claydo1@aol.com
Falk Rossberg
falkrossberg@t-online.de
Randy Kanary
rj@kanarysweb.com
Lenard Lof
alltech.transmissions@usa.net
Randy Kanary
kanarys@zbzoom.net
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Mileage: 87043
Repair History: Came in with no 4th Gear Rebuilt trans replaced 2-4 band & reverce input drum still no 4th gear
Work Completed: Check oil presure at idle 105 psi
Summary: 1-2 shift are fine 2-3 shift is slow about 35 mph at very little throttle then no 3-4 shift. It dose not have a neutral condition,just no 3-4 shift, But if you lift off the throttle at 60 mph it feels like it is in neutral then when you get back on the throttle it is in 3rd
John Sines
johnbsines@compuserve.com
Frank Choate
jfranklinc@aol.com
Leo Schneggenburger
lschneg1@rochester.rr.com
Keith Bruce
kwbruce@telusplanet.net
Roger Pryor
whizwheel@aol.com
Jeff Anglesey
apautooldtimer57@aol.com
Steve Allbee
steve@customtrans.com
John Sines
johnbsines@compuserve.com
Kenneth Bracy
transhop@localnet.com
Jim III
stardust@frontiernet.net
Roger Pryor
whizwheel@aol.com
Leo Schneggenburger
lschneg1@rochester.rr.com
Falk Rossberg
falkrossberg@t-online.de
Falk Rossberg
falkrossberg@t-online.de
John Sines
johnbsines@compuserve.com
CJ of-Canada
info@transtechca.com
Jim III
stardust@frontiernet.net
Frank Choate
jfranklinc@aol.com
David Foster
transtech@metrolink.net
Jeff Balak
kdhtrans55@aol.com
Paul Erickson
stp1paul@aol.com
Jim Eberhart
eberhart@efortress.com
Jeff Anglesey
apautooldtimer57@aol.com
John Sines
johnbsines@compuserve.com
Howard Johnston
hkj@sonnax.com
Kit Lindsay
lindsay2@sprintmail.com
Dean Mason
translab@juno.com
Anthony Petti
sburnout@aol.com
Gregory Gaal
gregg505@aol.com
Kim Walton
citytrans@webscene.com.au
Clayton Allen
claydo2@aol.com
Bob Ryan
firstrate@firstrate.demon.co.uk
Dell Wellons
woodchpr@worldnet.att.net
Leo Schneggenburger
lschneg1@rochester.rr.com
Chuck Clampitt
mrshift@starcomm.net
Steve Allbee
steve@customtrans.com
John Sines
johnbsines@compuserve.com
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Mileage: 120 k
Repair History: rebuilt last week
Work Completed: replaced pump, replaced VB, sep plate, gaskets
Summary: OK, since John has fixed his, here's my tale of woe:
Rebuilt unit, it came back not shifting.
Pulled back out, found pump slide looked like it was binding.
Installed rebuilt pump, did 10 mile road test, shifted great, next day it came back again.
Gage shows 140 at idle, same as before pump replacement.
Just got in from changing VB, started it, 60 pounds. Wow...its fixed......
NOT! after 3 blocks, it went back to 140.....very erratic, the gage is doing a dance between 100 and 160.....
Guess I'll pull it and replace with a shelf unit, unless anyone has any bright ideas.....I'm guessing cross-leak or crack in case, since that's the only thing not changed.
Gary Glaenzer
glaenzer@csj.net
Darwin Upton
darwank@usinternet.com
Leo Schneggenburger
lschneg1@rochester.rr.com
Kit Lindsay
lindsay2@sprintmail.com
Gary Glaenzer
glaenzer@csj.net
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Mileage: some
Repair History: Hello all, this truck is originally a 5spd with a 305 engine, now is a 383 with a 700R4 truck. Went from 3.73 to 4.10 gears, need to now if and where DRAC is.
Work Completed: If it doesn't have a DRAC it will have to get an ATG Recalibrater, to get the speedo correct. I looked under the dash briefly and saw no little white box. Manuals don't even normally acknowledge this wonderful little item.
Summary: If anyone knows if this truck has one and if so where is it located, if not I will have to give the Recalibrater a try. Thank you and have a good weekend.
Don Oremus
Kilpatrick Eng. & Trans
Waukesha WI
Don Oremus
dkoremus@execpc.com
Dan Tucker
transman@prodigy.net
Don Oremus
dkoremus@execpc.com
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Mileage: NA
Repair History: Cust say 3 transmissions in 3 years. Every time cust has installed himself. He has not bypassed the stock cooler. He just used flush in a can.
Work Completed: Bench job. Fluid is BLACK. Clutches look good. Overrun sprag worn out. Rear planetary carrier cracked. Planetary bearings shot.
Summary: Is it possible to build a trans to hold up to the turbo. He wants to to a 3000lb trailer. I am thinking cust low stall converter, Big Tru-Cool, .5 inch boost valve. Any other ideas or input? I am concerned about lock-up holding up to the power. Since it comp controlled, I can't put in the conv delay valve. I read one of you guy installs 700's in Suburbans without a lock-up clutch. Is this idea worth consideration? I know there is a wide range of opinions on this topic. Thanks a bunch. No I mean a whole bunch.
Daniel Wills
danwills@mindspring.com
Darwin Upton
darwank@usinternet.com
Chuck Clampitt
mrshift@starcomm.net
Leo Schneggenburger
lschneg1@rochester.rr.com
Daniel Wills
danwills@mindspring.com
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Mileage: 150.000mls
Repair History: none
Work Completed: none
Summary: I need pictures of this transmission in order to locate parts.
There is one clip or retainer near the park-lock whichi dont know where it came from! I have no sectional picts of that tranny whatsoever.
Erik Schulte
schulte@schulte-automobiltechnik.de
Erik Schulte
schulte@schulte-automobiltechnik.de
Pete Morgan
pjm59@worldpath.net
Harold Hawkins
harolds1@flash.net
Erik Schulte
schulte@schulte-automobiltechnik.de
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Problem/Fix: I have been swapping auxillary VB unit and non-Aux unit almost forever, with absolutely no problems. I intend to do that on this one. The only difference beside AUX is the Aux has 30 spline torque converter and the one non-Aux that I intend to install has the old 27 spline. The question is will this present any installation problems. The vehicle will also receive a separate Tru-cool cooler. Thanks, Jim, III
Jim III
stardust@frontiernet.net
Problem/Fix: Jim III, I think the weak link in this conversion would be the input shaft, if the van is to do any hard work Emory
Don Emory
mwolfing@vicon.net
Mileage:
Repair History: Rebuilt and airchecked, no shortcuts.
Work Completed: Non-perfect road test.
Summary: 700R4 Non-aux-VB.
1-2 nice shift
3 makes the shift and then is neutral or spin-up
then will go into 4th.
Now the 3-4 clutches have to be on to get 3rd or 4th. So I'm assuming the
3-4 clutches are working.
TV is stuck with no line rise at about 75#
The only thing that I can think of is that is not enough pressure to hold
3rd. 4th only requires 75 or 90# to hold it.
I have installed the cup plug in the servo. any thoughts. Jim, III
Jim III
stardust@frontiernet.net
Billy Tippit
batippit2@cs.com
Dell Wellons
woodchpr@worldnet.att.net
Kent Nelson
kent@mich.com
Jim III
stardust@frontiernet.net
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Mileage: NA
Repair History: Not knowen
Work Completed: Tear down, stop by mud
Summary: OK- I will try this again. Has anyone done work on a trans that
has been in flood and has set for 6-12 months?? I have a 700R4
I was going to build for stock but have been unable to do much
to get it cleen. Any suggestions? as I am ready to junk it.
Larry Williams
Tucson, Arizona
Larry Williams
maxiepoo2000lw@netscape.net
Gary Glaenzer
glaenzer@csj.net
Daniel Wills
danwills@mindspring.com
Tony Yurkevicius
trannyman123@aol.com
William Chechel
wchechel@aol.com
Dan Tucker
transman@prodigy.net
Dave Hocanson
hsp@bright.net
Larry Williams
maxiepoo2000lw@netscape.net
Larry Williams
maxiepoo2000lw@netscape.net
Larry Williams
maxiepoo2000lw@netscape.net
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Mileage: 98000
Repair History: none
Work Completed: none
Summary: I am building a 700R CORE none auxiliary vb, with a (type 4 Wiring Diagram MODEL: FA, MA, MM, TJ, YK, YN, YP,YT) for a costumer who is going to put in a 57 CHEV with a CHEV 350 engine. He would like not to have the lockup converter option.
Questions:
1. Anyone installed converter without a lock up clutch in a 700r?
2. If the question to 1. Is yes what has to be done to the lockup part of the
Hydraulic system if any?
3. What about the electrical part of the trans?
4. Anything that I didn’t mention?
Thank you for you input.
Walt
Walt's Trans
waltg@relia.net
Don Emory
mwolfing@vicon.net
Leo Schneggenburger
lschneg1@rochester.rr.com
Pete Morgan
pjm59@worldpath.net
Billy Tippit
batippit2@cs.com
Ken Buehler
kbuehler@freespace.net
Walt's Trans
waltg@relia.net
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Mileage: 91000
Repair History: Overhauled trans 30 days ago with kit and converter, pump Came back with no/late upshifts, dropped pan, metal,,,Converter went bad,dropped bearing, put metal in trans
Work Completed: rebuilt again, now no upshift at all, replaced case didn't like some things about it,put in sometimes late upshifts again, replaced valve body and installed tv spring,works 90% of time but when hot it has an occasional late upshift and maybe no od at all, also does it after useing reverse it seems..pull over bang pedal a few times and back to working perfect
Summary: what would you guys try next?
Dennis Gipe
dgipe@cvn.net
Ronnie Bingham
mrtrb@bellsouth.net
Daniel Wills
danwills@mindspring.com
Leo Schneggenburger
transfixleo@netscape.net
Steve Allbee
steve@customtrans.com
Dennis Gipe
dgipe@cvn.net
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Mileage: ?
Repair History: Trans was built for this hotrod.
Work Completed: Rebuilt unit with new converter. master kit & bushings & filter.
Summary: On this unit, torque converter came apart, filling unit with fine metal. After overhauling , this trans has a pronounced knocking noise anytime the pressure rises above 150 PSI.
I took pressure tests as follows.
P 100 230
R 155 280
N 100 230
OD 100 230
D 100 230
2 205 205
1 205 205
As you can see, I have good boost. When the pressure passes 150 PSI, it starts to knock like a broken flexplate. Only thing is, whren it passes 260 PSI, It shuts up! I thought I would run this by you guys before I shoehorn this thing back out(PITA)
Thanks in advance.
Paul Davies
phdavies@theramp.net
Dave Hocanson
hsp@bright.net
Leo Schneggenburger
lschneg1@rochester.rr.com
Falk Rossberg
falkrossberg@t-online.de
Paul Davies
phdavies@theramp.net
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Problem/Fix: need to know if no tcc will cause trans to overheat and burn 3-4 clutch, also need copy of bulitine.
Ronald Abbott
merle7@bellsouth.net
Mileage: 100,000 ?
Repair History: Muffler shop replaced 3 seals, then I got it. Removed pump, replaced worn conv. to pump bushing, enlarged drain back hole to 1/4 inch,cleaned & checked p/r & boost valve, re assembled pump and installed w/new gasket,seals and rings.
Work Completed: Muffler dudes reinstalled it and drove it,said it was fine. Customer didn't make it out of the lot and it started spewing oil again. they put it on the hoist and said it was the seal again.
Summary: They are dragging it in here tomorrow. Could someone please refresh my memory on why these seals blow out. Oh yeah, its got the seal retainer on it too. The seal fits tight and the pump is in great shape. Trans shifts good according to the owner.
Dave Hocanson
hsp@bright.net
Tom Whitty
twhitty@nji.com
Donald Stone
aaatrans@treco.net
Robert Bruce
robertlb@ev1.net
Roger Pryor
whizwheel@aol.com
Leo Schneggenburger
lschneg1@rochester.rr.com
Steve Allbee
steve@customtrans.com
Dave Hocanson
hsp@bright.net
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Problem/Fix: Well the 700-R4 has finally done it. Gotten old like the Powerglide of years past. We had 2 of these this week and have been fighting it for a couple days. These tranny's are getting high mileage and have been rebuilt numerous times. We found the problem, it drops the 3-4 clutch. The input shaft is becoming loose where it presses into the drum, and the 3-4 clutch feed is very close to the edge. When very carefully air checking, we found it leaking at that point, and the hotter it gets the more it leaks. We condemned 4 drums today. We put them in the parts washer for a few minutes and they really leak. Just thought you might like to know.
Frank Choate
jfranklinc@aol.com
Mileage: 138,000
Repair History: trans rebuilt by someone else 6 months ago
Work Completed: test drove,checked for power to tcc switch.
Summary: hi group, cust brought truck in and said that trans had been rebuilt
about 6 months ago.he has a late shift on the 2-3 shift and no tcc
but he has replaced feedback Q-jet with a carter and has butchered
the cable and the vacume lines to the tcc vacume switch.my question
is since he has replaced the carb and he expects me to wave my magic
wand and make it all better,does the tcc vacume need to be manifold
or ported vacume. any help will be greatly app.
thanks to all
bryan mead
reliable automotive & transmission
oak grove mo 64075
b.l.mead@worldnet.att.net
Bryan Mead
b.l.mead@worldnet.att.net
Clayton Allen
claydo2@aol.com
Steve Robinson
gearhead2@webtv.net
The author's membership with TRNi expired. Therefor, the thread was closed with no fix.
Mileage:
Repair History: owner try to rebuild the trans
Work Completed: n/a
Summary: When I got this trans it was all mix up early & parts got it all back together same year parts works nice BUT the oil pressure goes cazys at ilde 65 in park give it some gas rise to 75 come back down ok right ? So I drive it oil pressure goes 120 to 0 to 100 back down 0 it does it so fast that I can hear the needle on the gauge hitting againtist it self !!! So What the hell is it ?
Robert
Robert Mata
j200tm@starquest.net
The author's membership with TRNi expired. Therefor, the thread was closed with no fix.
Mileage: 98,000
Repair History: none
Work Completed: did oh relaced tc,bushings,band,shift kit,etc.
Summary: after oh it worked fine after about a month on the road it ame back when it goes into lu its ok but when your doing 60mph then leave off the gas and coast to about 50mph then step into it again when lu applies it vibrates like crazytouch the brake its goneonly thing i did so far was to put dr. tranny additive in it told customer to call me tuesday and let me know like some ideas on this one thanks,
Gregory Gaal
gregg505@aol.com
Billy Tippit
batippit2@cs.com
Roger Pryor
whizwheel@aol.com
James Leal
jcaphook@aol.com
hi fellow members,i posted this problem a week or so ago i had a reply from someone who said they could tell me exactly what lock up spring to use but i cant find who it was must have deleted it by mistake.this is a 85 gmc safari van v-6 after we oh. it it goes into lock up fine but after your going about 55-60 mph and let of gas then step back on it vibrates bad first thing i did was to put dr.trannys additive in it didnt help, so vans coming back tomorrow would like some info on this please thanks.
Gregory Gaal
gregg505@aol.com
ignition miss under load very common causes shutter/vibration light brake petal {enough to light brake lamps}during shutter if it comes+goes with brake on/off most likely ign miss good luck
Webster Dave
drwtt@wtco.net
Gregory. Put in the red spring from the 200 SK (it is for the accumulator valve) That will give you 11 pounds. I have gone up to a 16 pound spring with no ill effects. It will also raise LU and you will have a stronger apply. Jim, III
Jim III
stardust@frontiernet.net
jim thans for the info i used the red spring like u said that did the trick thanks again.
Gregory Gaal
gregg505@aol.com
problem was fixed thanks again jim closing thread now.
Gregory Gaal
gregg505@aol.com
Mileage: 250,000
Repair History: overhauled this trans about a year ago and it has worked fine.
Work Completed: verify complaint works great untill you go full throttle
Summary: if you shift this transmission into nuetral reverse or park, then go back to drive it works fine again. untill you go full throttle. What do you say guys? any help here. my plan is to pull the valve body and look at the t.v. plunger.
Jeff Anglesey
oldtimer57@hotmail.com
Frank Choate
jfranklinc@aol.com
Falk Rossberg
falkrossberg@t-online.de
Robert Bruce
robertlb@ev1.net
replace case and valve body
Jeff Anglesey
apautooldtimer57@aol.com
Mileage: all
Repair History: none
Work Completed: none
Summary: looking for interchange. for years I have interchanged these never worring about it just aux valvebody and none. then pwm . I have a bunch of core stuff, and want to build some completes. as I look I see a area around the screen on the cover that on some have a hole with a orface plug in it. others have a dam then that hole is not pluged. it looks like a guy could miss match and have a severe leak of pressure. has any one had any experance with this? Jeff
Jeff Anglesey
apautooldtimer57@aol.com
Gary Glaenzer
glaenzer@csj.net
thanks for all your help
Jeff Anglesey
apautooldtimer57@aol.com
Mileage: 120,000
Repair History: none
Work Completed: Balanced rear driveshaft twice, replaced rear shaft. Changed all mounts, changed pinion angle.
Summary: I am posting this for a friend. This all wheel drive van has a vibration that starts around 40 mph and doesnt go away. You can feel it right through the floor and seat (swear it was drivesahaft).if you remove the front shaft, nothing changes. He phoned a gm techline and they said something about a transfer case bulletin concerning this. Anyone heard of this. Any fresh ideas appreciated.
Mike Quigley
mikeq@netcom.ca
Darwin Upton
darwank@usinternet.com
Pete Morgan
pjm59@worldpath.net
No fix. just closing thread.
Mike Quigley
mikeq@netcom.ca
Repair History: Rebuilt unit 3 years ago
Work Completed: Unit needs OH. Rebuilding now
Summary: This truck has been converted from a diesel to 454 w/Edelbrock high rise manifold, and performer carb (kinda' like a Carter AFB)
TV cable is all cobbled up, and I'm sure improper tv pressure is the reason for unit failure.
What is the rule of thumb when trying to get the cable mounting bracket, and angle of throttle lever set right? Why do people have to butcher thier cars????
Thanks
Pat@Transmission Technicians
Niles,MI
Patrick Chamberlain
patrickcpatman@aol.com
Pat, We usually install a universal cable so we can adjust the center distance from the bracket. We then use a tv cable kit part#81-909S from transtar which is a spring/retainer carb end. This combination will cure your problem. Etranz
Ernest Spear
etranz49@gte.net
Patrick, We did an 88 diesel to 454 conversion 2 years ago. Fought the TV adjustment for DAYS!! Napa has a cool cable bracket available, part # 7352458. Good luck !
Jeff Johnson
pctm@turbonet.com
I think I got enough info Thanks all!
Patrick Chamberlain
patrickcpatman@aol.com
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Mileage: NA
Repair History: Not Known
Work Completed: None
Summary: This man who owns this Astro van is coming in AM to buy
a 700R4 I have built for stock. My question is my valve body
has only 1 switch, his is unknown. Should I pull his valve body
and electric and switch to my trans if there is a difference
or will it work anyway. I have this feeling it won't work!!!
I need an answer right away!!!
Larry Williams
maxiepoo2000lw@netscape.net
Donald Stone
aaatrans@treco.net
Dale Blake
dblake@telusplanet.net
Gary: Hindsight is always 20/20, so I will wait to tell you how I handle the situation you are in (business-wise) and only deal with the techncial issue at hand. Carburator geometry is critial for proper pressure rise. 132psi @ WOT is not enough. From your description, it seems like you have a slow, or lazy, pressure rise. I would be willing to bet the 4X4 truck does not have the factory intake, carb, or linkage & bracket. -or- a combination of the previously mentioned. Questions to help the group diagnose your problem: 1. Does it have a 2-1 forced downshift? 2. Is the carb, intake, TV/throttle bracked & TV cable OEM? After we have that information, we can intelligently help you out of the bind you're in. Anxiously Awaiting To Help You,
Larry Bloodworth
larry_b@certifiedtrans.com
Hi Gary, With these early 700's I would use Gils noyoyo kit,this kit fixes alot of the shift timing problems as well as be able to void(block off) the tcc solenoid so that lock up works without being commanded electrically (it takes longer to fit than the jnr but its worth the extra effort). Your line pressure rise is lazy (considering the jnr kit increases line pressure by about 15% from std)so you need to address that problem maybe it is in the cable set up and that may cure the shift flair,try the max test making sure the cable/tv is at full travel.The third flair could also be caused by the check ball capsule in the servo housing if it is worn it may be affecting the shift timing from 2nd to 3rd,you can change the capsule (differcult while in the vehicle)or fit a sonnax check valve #77701-076 behind the capsule to correct the timing of the shift(you can also increase the third orifice in the v/b plate to get quicker/firmer apply.Also the .100" 3/4 clutch clearance would probably not be helping,I like to run .025"-.040".Hope this helps you out,good luck! Regards Kim PS. With the Jnr Kit I've never been able to fit the spacer washer behind the 2nd servo I always end up grinding the apply pin down to get the band clearance right(1/16" pin travel).
Kim Walton
citytrans@webscene.com.au
Gary, the tv rise problem needs to addressed first.You need to check the tv geometry and correct it in order to go any further.#1 make sure the carb has full throttle with the pedal to the floor and fixed if not so. #2 with the throttle at wot the tv cable must be pulled to max movement and you should check this with the pan off for a visual conformation and correct it or you will be chasing your tail. You didn't tell us what carb was being used on this truck,If it is a holley some of them had the wrong ratio for the tv cable pull pin ,to far away or close to thr throttle shaft center line.Sonnax makes a corrector lever for this but it may not be right for this. If the carb is oem replacment rochester you should be ok. Once the tv relationship is good 68# min line is ok but max line shuold go to around 175 -210 psi in drive and 90psi min and 250-275 psi max line in reverse.Don't try to fix shift problems until line rise and fall is correct ,again tail chasing syndrome. I too like close tolerances on the 3-4's around .025-.040.This will help reduce 2-3 flairs but not fix them. the vette piston will correct most 2-3 flairs but not all of them. If you reset the 3-4's you will be happier with the results from the vette piston route. The 3-4 shift valve assy may not be needed once the line rise is working .The truck should have the needed electrical to work the T/C if it still works and if not use the tech and parts in the 700 green box kit to make it work and calibrate it to the desired road speeds.In the younger kit hole C is 3rd gear feed and to big of a hole (more than .110 ) will make 3rd soft or loose felling at light to med throttle and stay around .083 - .086 on hole B . I hope this helps
Dwight Armstrong
dlarmst@juno.com
Rechecked Line Pressure With new gauge. 65# at Idle in N. Full TV at Idle in N. 160#. Same Readings in DR. Rev. 105# Idle, 230# Full TV.
Carb. is Quadrajet, Braket is off factory Engine, pulled pan to make sure Cable was pushing plunger all the way in at full throttle and it is.
It does do a Forced 2-1 downshift. The trans is a TK type 1 Wiring in the ATSG Manual, For help on Tcc, Ordered Vette Servo and sonnax valve will install on arrival, Is that Gils noyoyo kit something I should do instead of wiring through brake and pressure switch on VB ??
Also I found that the filter was very loose in pump bore and O-ring, will replace.Thank so for for the help.
Gary Nelson
nelsonauto@hotmail.com
The large green Transgo kit works very good, especially in the early units that used all the valves. I prefer to set them up with the diesel/ 2.8 springs in all of them as it makes for a slightly later 3-4 and lock up. I do not like the way they work with the check ball installed in the TCC solenoid, although the trans will work. They work much nicer especially on on forced downshifts if you take the time and correct the TCC electrical system properly.
David Schaffel
dbschaffel@home.com
Gary, when I build most any non-aux unit I will use the noyoyo kit and the 700-JR on the aux units. The only time I really use the lock-up bypass is when the car is not equipt for it or it dosen't work otherwise I try to use the factory stuff. Now I was fliping through my car mags. and low and behold a company called painless wiring build a kit for the GM lock up control around ...oh hell now I can't find it O well
Dwight Armstrong
dlarmst@juno.com
Got a Problem installing sonnex valve 77701-076, per instructions tapered end of valve installs into case,and should be driven in flush with or in a little from valve body surface, OK, My hole is to big valve slides up hits capsule and will fall back out. What's the Problem?????
Gary Nelson
nelsonauto@hotmail.com
Hi Gary, I don't know why the sonnax servo check valve is loose in the case never had that problem.Obviosly you can't use it in this trans.I would extract the capsule and fit a new one.You can exact it using a 5/16 tap or a #5 easy out and a small slide hammer and install it using a old 700 PR valve as a driver and when the wide end of the valve is flush with the case the capsule is installed correctly, learnt this trick from Jim III.Hope this helps you out,good luck!!! Regards Kim
Kim Walton
citytrans@webscene.com.au
Sonnex Valve, Welded end and remachined, hole in case was .010 bigger then valve, Valve worked fine after welding, If valve didn't fit, I figured the capsule wouldn't, so I tried this and it worked. Also found out that friend of customer, Installed His own design VB spacer plate, Left out Detent and low Check ball and install Spring first then piston in 3-4 Accmulator, anyone done this??, and way. Only thing I could see he did on plate was open 2-3 feed to .140 witch is Ok now, since I am Installing Corvette servo and Sonnex valve, Trans is a Tk 1983, Still Need to Know how to hook wires to pressure valves on VB for TCC, No longer has computor, Thanks for help so far.
Gary Nelson
nelsonauto@hotmail.com
Gary: If I understand you correctly, you are asking how to connect the wires on a unit that is no longer computer controlled. It doesn't matter. If the electrical system is no longer functioning, it is a futile attempt. On such units, I use TransGo's Shift Kit and put a 5/16" checkball in the snout of the TCC solenoid as instructed. However, if you use the checkball in the snout of the TCC solenoid w/o the the Shift Kit, I have experienced L/U right on top of 2nd. Plus, there is no part-throttle release of the TCC. Just break down on Monday and order the TransGo Senior Shift Kit (not the Junior). It will make life wonderful; I promise. Also, with this kit, and no functional computer system, you can put 1/8" pipe plugs in all of the electrical switch holes in the valve body....clip the wires off the TCC solenoid, and forget about any electrical problems, FOREVER. :-) Sincerely,
Larry Bloodworth
larry_b@certifiedtrans.com
Gary In addition to what Larry said, make sure the valve body you are using has a lock-up shift valve. If it does not have a lock-up shift valve the trans will lock-up on top of the 1-2 shift. Use the heavy lock-up spring in the Shift Kit. A corvette servo may make your 2-3 flair worse. A Sonnax servo valve may correct your problem. If you use a Corvette servo, don't forget to drill out the Sonnax valve if you have to use one.
Jim Eberhart
eberhart@efortress.com
Hi Gary, I just read your last update and it seems that there is alot more problems in this trans due to your customers friend mucking around with things.I just love these ones:-( This is what you could try,if you fitted a junior kit set it up exactly how the instructions show (green box would be my first choice), correct anything that has been changed by the customers friend.Your original flare was more than likley caused by the 3/4 feed being drilled to .140 (are you sure this guy hasn't drilled anything else? maybe you should replace the plate) anything over .090 can give you problems in this area unless you correct it, a sonnax valve check valve will do this,this trans will have a harsh 3rd shift at .140,I only go this far in a high performance application ,then when you add a corvette servo(don't forget to re drill the sonnax valve to suit) to that it will have a fairly bumpy 2nd shift as well,is this what your customer is looking for? If you what to carm it down then you can go down on the 3/4 feed .110-.120 with the sonnax valve and run a 4L60E 553 servo piston (better apply than the original 544 servo piston but not bumpy). In regards to setting up the lock up electrics,I think another member posted some info on that one,might be worth going back through the replies.Hope you can get this one down the road soon,good luck! Regards Kim
Kim Walton
citytrans@webscene.com.au
Thank You All that helped !!! I installed Gils Noyoyo, a 093 vette servo, had to make sonnex 3-4 accum. valve fit passage, and redesigned TV sleeve as described in one of your fixes,Trans works fine. Found more things Costomers friend did, thing you may not normally see. Again Thank You!!!!
Gary Nelson
nelsonauto@hotmail.com
Problem / Fix: Here's another discovery by accident. We had rebuilt this transmission in a 1984 Surburban w/ 6.2 diesel and on the test drive discovered that we had hard, nearly chirp the tires hard, 1-2 shift.
First we had a TV cable problem creating high line pressure, but after that was fixed we still had a hard 1-2 shift. Pulling down the valve body revieled that we had put a 3-4 shift spring in the 1-2 accumulator valve accidently while trying to recalibrate for a piston change.
I've used valve body kits before that would give a very firm 1-2 shift but this unit had a greater change in that spring than I've felt in doing a complete kit. No blocking off the accumulator piston or drilling out excessive holes.
Jimmy Taylor
odie@gci.net
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Mileage: 142000
Repair History: Trans rebuilt at 116000 went 16000 and had a lock up shudder replaced ness parts and now its back with same problem with only 14000
Work Completed: Cut converter apart and found clutch coming apart
Summary: Has any one had this problem? Any info will be of great help
James Schuler
goldenboys5@uswest.net
Replaced pump
James Schuler
goldenboys5@uswest.net
Repair History: rebuilt trans ,rear planet was gone do to lube problem rebult checked cooler flow
Work Completed: came back afeter less than 100 miles planet melt down no lube to gear train , clutches and band like new
Summary: what are we missing here
William Brenzel
gbren1425@aol.com
William, How about some details for us on what if any hardparts were used to build this thing 100 miles ago and what softparts used also this will help us help you better.
Dwight Armstrong
dlarmst@juno.com
Wrong lube dam seal in input drum, feed holes plugged in output shaft,, too much endplay, worn bushings. That is if cooler is still flowing OK. Also rear planet with oil deflector MUST be used with matching beveled support.
Chuck Clampitt
mrshift@starcomm.net
Hi William, I would check to make sure all your lube passages are clear in the output shaft. Double check the seal in the input drum. I think at this point, I would bypass the original cooler with a Tru-Cool. Good luck!
Daniel Wills
danwills@mindspring.com
When you havbe this kind of problem it makes good sense to change allthe bushings in the trans. Anopther thiong that I would do is to check the output shaft oiling ports to make sure that they are all clear . The third thing I would do is to make sure that cooling system is clear all the way from the outlet line to the cooler and then back into the trans. arIzzOna kid no I did'nt spell arIzzOna wrong .
Ronald Izzo
i220@juno.com
William, Take your output shaft and feed solvent into the top of it and see if it flows through every hole. Then do the same with the input drum where the lube seal rides. There must be a restriction in those two shafts. If not, check stator busings and tube for ring grooves. What condition was the lube seal when you pulled it back out? If it was tore up, suspect worn bushings. Did your planet train match up correctly? Another thing about the lube seals, since they came out with "lip seal", I have noticed more meldowns more so than the solid ones. They seem to be less tolerent of bushing wear than the solid types. If my kit only comes with the lip seal, I would hunt me down a solid type. In my mind, this is strictly a mechicanical problem since it only lasted 100 miles. I hpoe this helps. Butch
Butch Vipperman
rvipperman@kimbanet.com
Number one killer of planetaries is that plastic, serrated, (whatever the hell it is) that is in the input housing and mates with the output housing. Replace on every job. The older ones were white in color and the newer ones are red in color. Now the lube hole for the red (pink) has been moved and you are supposed to replace with that color only. (Do not know if this is true). Anytime I have a burned planet, it gets a Tru-Cool mounted separate from the radiator. Jim, III
Jim III
stardust@frontiernet.net
Bill: I think what everybody else said pretty much covers it all, but I though I would give you some thoughts. COOLER ISSUE: Unless your factory cooler was severely restricted, or the cooler lines were pinched almost shut, I don't see how the rear planet could crap out in only 100 miles. INPUT DRUM LUBE SEAL ISSUE: Unlike a lot of transmissions, the 700 gets fed it's lube from the front of the input shaft and the rear planet is at the end of the circuit. So what everybody is saying about bushings, oil holes, and the lube seal boils down to making sure you are loosing lube somewhere because the rear planet is at the "end of the line" as far as the rear lube circuit is concerned. WORTH MENTIONING: The is a bulletin our showing that GM changed the location of the lube hole in the front of the output shaft where it meets the input drum lube seal. Make sure you don't have a mis-match between the output shaft and lube seal. Good Luck,
Larry Bloodworth
larry_b@certifiedtrans.com
William, You've probably already checked this, but sometimes I have seen a trans get trashed and pack the shafts full and no lube can get through them. I have had some that I had to actually dig the trash out of them. Good Luck.
Roger Pryor
whizwheel@aol.com
Hi William, What everyone else said, plus... How is the vehicle used? If for some reason this is pushed to the point that it is under heavy load and L/U doesn't engage, this can happen. In some cases what is required is a lower rear axle ratio. Also, did you grind the PR valve as per the Shift Kit instructions?
Leo Schneggenburger
lschneg1@rochester.rr.com
Once you get this unit back into the vehicle, it's time to check the real flow of oil that's returning to the trans for lube. I just recently got a SonnaFlow & I don't know how I ever got along without it(especially for no more than it costs). When it comes down to it, I think you are going to find the pump on this thing, even though it looks good, has a poor output after it gets Hot. Combine that along with end clearence and bushing problems and you have the recipe for disaster. Most all 700's have way too much, Rear drivetrain end clearence is often looked, Slow Down, take a deep breath, and fix this thing!
Jeffery Funk
shiftkit@specialtytrans.com
Hi William We once replaced the stater in a 4L60 pump and found that the lube hole hadn't been drilled in it. It made it about 60 miles before it melted. If you repalced the stater in your pump then you should install it in the case and blow through the cooler oil return fitting to see if lube oil is passing through. Hope this helps. Kit
Kit Lindsay
lindsay2@sprintmail.com
origanly overhualed with rear planet, reverse drum , forward drum, do too cracks inside .overhaul kit and converter
William Brenzel
gbren1425@aol.com
Bill: What Leo said triggered a thought in my head. If the PR valve is not ground (line-to-lube modification), if the PR valve stays closed, or mostly closed, for ANY reason, it automatically shuts off lube oil by design. Just a thought worth mentioning. Sincerely,
Larry Bloodworth
larry_b@certifiedtrans.com
hi bill, i think u got some good info from everybody so far i just read that u replaced the forward drum was this a used one? maybe u got a bad one something wrong with lube circut on it, also talking about those lube seals ive been using the brass seals in there had no problems and holds output shaft in line pretty good.
Gregory Gaal
gregg505@aol.com
hooked up cooler line flusher that has line flow presure test with heated fluid , when the temp of fluid would rise the cooler flow would drop , my guess is this could be the hole problem.
William Brenzel
gbren1425@aol.com
Because the flusher flow readings will Lie to you, do yourself a favor & buy a sonnaflow, NOT A AD ! I don't know how We ever got along without it! Jeff
Jeffery Funk
shiftkit@specialtytrans.com
checked cooler flow , presure wnt down when hot replace with true cooler. vehicle went out and hasnt been back for over a week
William Brenzel
gbren1425@aol.com
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Repair History: I Rebuild Trans, Customer installed, When I Sonic cleaned it,Printed on top it said Remanufactoried For GM
Work Completed: Main line pressure test at Idle 68# and at Full TV 132# This seem OK, Trans Was buildt stock with a 700 Jr installed I did not install washer spacer in servo, was to tight, could not turn output shaft.
Summary: The owner put in a Carb. engine diched computor so I need to Know how to hook up TCC. Its installed now, fuse to brake switch,Brake switch to A terminal, Trans shifts OK 1-2, shift into third at about 50 mph, Sometime not always, I'll get a Short Flair When Shifting to third under med to heavy Accel., One Thing I Know I Did And Will not Do Again is Let 3-4 Clearance stay at .100 The ATSG Book gave me Tolerance Of .049 to .113 so I let it go at that, I Read a 2-3 flair problem in Fixed Data and Iam Going to try a Corvette Servo, Also If Kevin Perkins Reads This, Your Info on OD shifting at any throttle is something I would like to try on this trans, Send Pictures If you Could, I Think the 4th shift when I let up on throttle is a Misadjusted TV Cable, Being It didnt stick When I Did Pressure Test. ? I am Hoping to fix With out taking Trans out to close up 3-4 clutch Clearance. Any Advice, Thanks, Nelsonauto@Hotmail.com
Gary Nelson
nelsonauto@hotmail.com
Gary: Hindsight is always 20/20, so I will wait to tell you how I handle the situation you are in (business-wise) and only deal with the techncial issue at hand. Carburator geometry is critial for proper pressure rise. 132psi @ WOT is not enough. From your description, it seems like you have a slow, or lazy, pressure rise. I would be willing to bet the 4X4 truck does not have the factory intake, carb, or linkage & bracket. -or- a combination of the previously mentioned. Questions to help the group diagnose your problem: 1. Does it have a 2-1 forced downshift? 2. Is the carb, intake, TV/throttle bracked & TV cable OEM? After we have that information, we can intelligently help you out of the bind you're in. Anxiously Awaiting To Help You,
Larry Bloodworth
larry_b@certifiedtrans.com
Hi Gary, With these early 700's I would use Gils noyoyo kit,this kit fixes alot of the shift timing problems as well as be able to void(block off) the tcc solenoid so that lock up works without being commanded electrically (it takes longer to fit than the jnr but its worth the extra effort). Your line pressure rise is lazy (considering the jnr kit increases line pressure by about 15% from std)so you need to address that problem maybe it is in the cable set up and that may cure the shift flair,try the max test making sure the cable/tv is at full travel.The third flair could also be caused by the check ball capsule in the servo housing if it is worn it may be affecting the shift timing from 2nd to 3rd,you can change the capsule (differcult while in the vehicle)or fit a sonnax check valve #77701-076 behind the capsule to correct the timing of the shift(you can also increase the third orifice in the v/b plate to get quicker/firmer apply.Also the .100" 3/4 clutch clearance would probably not be helping,I like to run .025"-.040".Hope this helps you out,good luck! Regards Kim PS. With the Jnr Kit I've never been able to fit the spacer washer behind the 2nd servo I always end up grinding the apply pin down to get the band clearance right(1/16" pin travel).
Kim Walton
citytrans@webscene.com.au
Gary, the tv rise problem needs to addressed first.You need to check the tv geometry and correct it in order to go any further.#1 make sure the carb has full throttle with the pedal to the floor and fixed if not so. #2 with the throttle at wot the tv cable must be pulled to max movement and you should check this with the pan off for a visual conformation and correct it or you will be chasing your tail. You didn't tell us what carb was being used on this truck,If it is a holley some of them had the wrong ratio for the tv cable pull pin ,to far away or close to thr throttle shaft center line.Sonnax makes a corrector lever for this but it may not be right for this. If the carb is oem replacment rochester you should be ok. Once the tv relationship is good 68# min line is ok but max line shuold go to around 175 -210 psi in drive and 90psi min and 250-275 psi max line in reverse.Don't try to fix shift problems until line rise and fall is correct ,again tail chasing syndrome. I too like close tolerances on the 3-4's around .025-.040.This will help reduce 2-3 flairs but not fix them. the vette piston will correct most 2-3 flairs but not all of them. If you reset the 3-4's you will be happier with the results from the vette piston route. The 3-4 shift valve assy may not be needed once the line rise is working .The truck should have the needed electrical to work the T/C if it still works and if not use the tech and parts in the 700 green box kit to make it work and calibrate it to the desired road speeds.In the younger kit hole C is 3rd gear feed and to big of a hole (more than .110 ) will make 3rd soft or loose felling at light to med throttle and stay around .083 - .086 on hole B . I hope this helps
Dwight Armstrong
dlarmst@juno.com
Rechecked Line Pressure With new gauge. 65# at Idle in N. Full TV at Idle in N. 160#. Same Readings in DR. Rev. 105# Idle, 230# Full TV.
Carb. is Quadrajet, Braket is off factory Engine, pulled pan to make sure Cable was pushing plunger all the way in at full throttle and it is.
It does do a Forced 2-1 downshift. The trans is a TK type 1 Wiring in the ATSG Manual, For help on Tcc, Ordered Vette Servo and sonnax valve will install on arrival, Is that Gils noyoyo kit something I should do instead of wiring through brake and pressure switch on VB ??
Also I found that the filter was very loose in pump bore and O-ring, will replace.Thank so for for the help.
Gary Nelson
nelsonauto@hotmail.com
The large green Transgo kit works very good, especially in the early units that used all the valves. I prefer to set them up with the diesel/ 2.8 springs in all of them as it makes for a slightly later 3-4 and lock up. I do not like the way they work with the check ball installed in the TCC solenoid, although the trans will work. They work much nicer especially on on forced downshifts if you take the time and correct the TCC electrical system properly.
David Schaffel
dbschaffel@home.com
Gary, when I build most any non-aux unit I will use the noyoyo kit and the 700-JR on the aux units. The only time I really use the lock-up bypass is when the car is not equipt for it or it dosen't work otherwise I try to use the factory stuff. Now I was fliping through my car mags. and low and behold a company called painless wiring build a kit for the GM lock up control around ...oh hell now I can't find it O well
Dwight Armstrong
dlarmst@juno.com
Got a Problem installing sonnex valve 77701-076, per instructions tapered end of valve installs into case,and should be driven in flush with or in a little from valve body surface, OK, My hole is to big valve slides up hits capsule and will fall back out. What's the Problem?????
Gary Nelson
nelsonauto@hotmail.com
Hi Gary, I don't know why the sonnax servo check valve is loose in the case never had that problem.Obviosly you can't use it in this trans.I would extract the capsule and fit a new one.You can exact it using a 5/16 tap or a #5 easy out and a small slide hammer and install it using a old 700 PR valve as a driver and when the wide end of the valve is flush with the case the capsule is installed correctly, learnt this trick from Jim III.Hope this helps you out,good luck!!! Regards Kim
Kim Walton
citytrans@webscene.com.au
Sonnex Valve, Welded end and remachined, hole in case was .010 bigger then valve, Valve worked fine after welding, If valve didn't fit, I figured the capsule wouldn't, so I tried this and it worked. Also found out that friend of customer, Installed His own design VB spacer plate, Left out Detent and low Check ball and install Spring first then piston in 3-4 Accmulator, anyone done this??, and way. Only thing I could see he did on plate was open 2-3 feed to .140 witch is Ok now, since I am Installing Corvette servo and Sonnex valve, Trans is a Tk 1983, Still Need to Know how to hook wires to pressure valves on VB for TCC, No longer has computor, Thanks for help so far.
Gary Nelson
nelsonauto@hotmail.com
Gary: If I understand you correctly, you are asking how to connect the wires on a unit that is no longer computer controlled. It doesn't matter. If the electrical system is no longer functioning, it is a futile attempt. On such units, I use TransGo's Shift Kit and put a 5/16" checkball in the snout of the TCC solenoid as instructed. However, if you use the checkball in the snout of the TCC solenoid w/o the the Shift Kit, I have experienced L/U right on top of 2nd. Plus, there is no part-throttle release of the TCC. Just break down on Monday and order the TransGo Senior Shift Kit (not the Junior). It will make life wonderful; I promise. Also, with this kit, and no functional computer system, you can put 1/8" pipe plugs in all of the electrical switch holes in the valve body....clip the wires off the TCC solenoid, and forget about any electrical problems, FOREVER. :-) Sincerely,
Larry Bloodworth
larry_b@certifiedtrans.com
Gary In addition to what Larry said, make sure the valve body you are using has a lock-up shift valve. If it does not have a lock-up shift valve the trans will lock-up on top of the 1-2 shift. Use the heavy lock-up spring in the Shift Kit. A corvette servo may make your 2-3 flair worse. A Sonnax servo valve may correct your problem. If you use a Corvette servo, don't forget to drill out the Sonnax valve if you have to use one.
Jim Eberhart
eberhart@efortress.com
Hi Gary, I just read your last update and it seems that there is alot more problems in this trans due to your customers friend mucking around with things.I just love these ones:-( This is what you could try,if you fitted a junior kit set it up exactly how the instructions show (green box would be my first choice), correct anything that has been changed by the customers friend.Your original flare was more than likley caused by the 3/4 feed being drilled to .140 (are you sure this guy hasn't drilled anything else? maybe you should replace the plate) anything over .090 can give you problems in this area unless you correct it, a sonnax valve check valve will do this,this trans will have a harsh 3rd shift at .140,I only go this far in a high performance application ,then when you add a corvette servo(don't forget to re drill the sonnax valve to suit) to that it will have a fairly bumpy 2nd shift as well,is this what your customer is looking for? If you what to carm it down then you can go down on the 3/4 feed .110-.120 with the sonnax valve and run a 4L60E 553 servo piston (better apply than the original 544 servo piston but not bumpy). In regards to setting up the lock up electrics,I think another member posted some info on that one,might be worth going back through the replies.Hope you can get this one down the road soon,good luck! Regards Kim
Kim Walton
citytrans@webscene.com.au
John: Converter runout, as in the 3 pads aren't running true. Drilling line-to-lube and having wide fluctuations in the converter pressure. Bent or out-of-square flywheel mounting flange on the crankshaft. Hey.....gotta go....I'll finish this up later..
Larry Bloodworth
larry_b@certifiedtrans.com
Hi John, Is it breaking around the crankshaft or at the converter bolts? I would suspect a high frequency vibration. Sincerely.
Roger Pryor
whizwheel@aol.com
John, I would be changing the torque converter and flywheel at this time. I feel you have a converter problem seeing you have checked everything else. Also be sure there is no pilot bushing in the back of the crank. I had a Ford Bronco 2 do this to us 4 times and finally changed the converter and it never came back and it was the original converter until the last flywheel. We assume that the converter was balloning and not able to move in and out of the crank on acceleration. Instead it flexed the flywheel until it broke the center out every time.
Donald Stone
aaatrans@treco.net
John: Sorry I cut you off on my last post, but I had to go. The most important thing I wanted to say; I didn't because I had to go. Here's the deal: GM has some weird thought processes. On a lot of what I call "the flat-top bellhousing" applications, they have crankshaft spacers. This applies to rear and front wheel drive transmissions. There is a sintered iron insert (sort of looks like a pilot bushing for a standard, but not) that is pressed in the end of the crank. I have run into situations, especially with rebuilt cranks/motors where this is missing. This crankshaft spacer not only centers the flywheel to the crank, but it also is the pilot hole for the torque converter. Make sure the crankshaft spacer is in the end of the crank; not damaged; and not worn out. ATC sells these seperately, or you can get one from the dealer. As previously mentioned by Don Stone, inside this same spacer I'm speaking of, you could possibly have a standard transmission pilot bushing installed and not realize it. Before you install the transmission, I would take only the converter and see how it fits in the crank and against the flywheel WITHOUT the transmission. That will probably identify your problem. Sorry about taking so long to get back to you. Sincerely,
Larry Bloodworth
larry_b@certifiedtrans.com
I am sorry to say that I have no real fix. The customer came by in a new Yukon to pay her bill. All we did was replace the flywheel. I'm sure it will again. If you are car shopping in Maryland, beware of a blue and white Blazer.
John Lovell
ent@crosslink.net
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Repair History: rebuilt by someone else who changed the case to a auxillary case with non auxillary parts
Work Completed: changed back to a non auxillary case during the rebuilding of transmission and install a transgo jr 700 r4 kit.
Summary: this vehicle shifts too quick no matter where you set the throttle cable. put another throttle cable on this vehicle but did the same thing. any one out there who had this problem please, please help.
Janice Easter
hun6@juno.com
I had one do this several years ago and it turned out that someone had installed a 350 governor, or maybe it was a 400 governor with the gear changed. Cant remember. However...I changed the governor and cured the problem.
Tommy Painter
county9@yahoo.com
One other thing if the gov, doesn't take care of it. Feel the cable and see if it might have too much tension. I have had some problems with the "no-stick" throttle vavle spring getting loose and stooping the stroke of the throttle valve. Good luck, Yogi
Jeff White
stealth@mscomm.com
Janice: Put a pressure gage on this pupply and get back with readings. If I had to make a guess, I would be looking at TV limit valve or TV valve stuck rearward. Jim, III
Jim III
stardust@frontiernet.net
Hi Janice, Check the governor to make sure it is free. If it is, try weaker governor springs. Good luck.
Roger Pryor
whizwheel@aol.com
I have not read this entire string, but the first thing i would check after all these other suggestions, is the valve body gaskets. 700"s can do weird things with wrong vb gaskets, reversed gaskets,and dont forget some 87"s that were not aux vb use aux vb gaskets. Good Luck!@
Bruce Bekkerus
a1mhd@aol.com
Janice, If it's a 4x4 make sure it isn't in low range. I know my manager wouldn't know. Bill
William Pihl
drcheckball@webtv.net
Hi there - the only thing I can think to add on this is regarding the transgo sk. Make sure you don't use the tv valve provided if your tv plunger is stamped with a 93. I did this a few years ago and for the life of me can't remember the resulting symptom except that it affected tv pressure. Good luck!
Michelle Oberg
trannychic@aol.com
this vehicle originally had a 305 engine in it but the customer put a 350 engine with a 4 barrel elderbrock carburator. I have changed the governors and also put another cable on this vehicle. In rebuilding the unit I installed a rebuilt pump from Dacco/Detroit which in which I had to use my own valves (tv,lockup,etc) to complete the pump assembly. Also a torque converter was installed in here also. This vehicle makes me think that someone has died in this vehicle. My rebuilder has never had a 700 to kick him like this. I thank you all for your input but none has worked. He knows about the 93 tv. any other help you all can give me will be greatly appreciated.
Janice Easter
hun6@juno.com
I still would like to have some pressure readings. It would sure eliminate a lot of guessing. You mentioned that you put in another pump. Was the black filter that is on the outside of the pump reinstalled. The filter is black and about the size of a nickel. Not reinstalling this filter will cause the symptoms that you have. Jim, III
Jim III
stardust@frontiernet.net
Jim he has installed the black filter back in the pump. The line pressure readings are as follow: Idle---------90 Reverse------80 Drive--------80 Upshift------95 This vehicle rack test good but when you take it for a test drive the shifts are just too quick.
Janice Easter
hun6@juno.com
Janice: Head right to the TV limit valve. Good luck, Jim, III
Jim III
stardust@frontiernet.net
Janice, Do you have line rise. pressure test and pull out the cable. If not the slide could be stuck in the pump.
Steve Allbee
sallbee@worldnet.att.net
just had the same problem, replace the govenor with a new one
Ernest Gaddis
egaddis@bellsouth.com
I would like to thank all that responded to my problem but special thanks goes to JimIII. The rebuilder put the wrong spring in the tv limit valve. This spring was in the transgo jr kit. Mixed with the accumulator spring I believe. Again, thank you Jim. This was the real fix.
Janice Easter
hun6@juno.com
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Repair History: Customer replaced dash with exchange unit because speedometer was working intermitant.
Work Completed: Installed Rebuilt trans. Road test confirmed no Lockup. Hooked up Shaeffer and confirmed the problem is not in the transmission. Scanner shows no vss signal and speedometer on scanner shows 0. Speedometer in dash works fine. Cruise Controol does not work.I have code 24 VSS circuit. I tried a known good ECM and same thing.
Summary: I believe my problem is somewhere in the DRAC. But I don,t get to work on the vehicles very often so I don,t know how to tell for sure.Maybe someone could help me out here?
The customer is from out of town and wants his truck. If it is the DRAC he wants to get warranty from the place he got the dash from.
Can I or should I connect the 4th gear switch directly to the ground side of the Lockup solenoid to get this guy going. What are the major side effects to doing this?
I don't want to let him take his truck without lockup and he doesnt want to spend anymore time or money in this town if the problem was caused by the replacement dash. Thanks in advance.
Dale Blake
Elbow Automatic Transmissions
Rocky Mountain House, Alberta,Canada
Phone:403-845-2784
Fax: 403-845-4983
dblake@telusplanet.net
Dale Blake
dblake@telusplanet.net
Hey, Dale: Dan Tucker ran in to this same problem a while back. Check out: http://www.transbuilder.com/trni/z_fix99/4l60a.html#50 He says the VSS wire breaks INSIDE the insulation and is very hard to diagnose. We had one that nearly ate us alive with the same problem. We sent ours to the dealer and they put in a new ECM, DRAC, and wiring harness. -PLUS- 2 VSSs. before they figured it out. The fix for this is listed in the TRNi Fix Database. Good Luck,
Larry Bloodworth
larry_b@certifiedtrans.com
Thanks Larry. I checked the fix database before I made a post. The first thing I checked was the wires under the vehicle. I pissed around pulling all the wires out of there looms and then realized I would not have a working speedometer if I had a broken wire. Thats the way I figure it anyway, I could be wrong. Dale Blake Elbow Automatic Transmissions Rocky Mountain House, Alberta,Canada Phone:403-845-2784 Fax: 403-845-4983 dblake@telusplanet.net
Dale Blake
dblake@telusplanet.net
Dale, If this guy is beating you up to get his truck, I would wire it as you say to get L/U in 4th. I also would document the heck out of the procedure you went through, and have him agree to hold you harmless. I can see it now, the guy gets home 200,000 km from your shop, takes it to a local shop, then wants YOU to pay to "put it back the way it's supposed to be." Good luck!
Jeff Johnson
pctm@turbonet.com
Dale, If I was the customer I would want my PCM to know the VSS. Because the scanner is not seeing the MPH, I doubt if the PCM realizes that the vehicle is really moving. Timing, fuel mileage, and all kinds of performance issues could come into play without a VSS in the PCM, beside the TCC apply. If this is indeed the case, fixing the problem becomes more important. I suspect that you have a problem in the wiring from the instrument cluster to the PCM. I'm not sure of the pin number at the cluster A17??, but the wire is brown (or brown/white) I think, and it runs to the PCM's pin A10. I've seen the wire broken at least twice. I never have dug into it to find out why, I just run a new wire. One last note, if the speedometer has been replaced, make sure it is the right one. MOST of the 1989 have the white bar behind the rib speedometer. The speedo needle looks like a picket fence. MOST the 1990 models have the white bar that is fully exposed with a bright red or orange line to show the speed. I know this sounds crazy but there are 2 different speedometers, and they will fit, but not work right. I think the buffer part is the only difference. I think the speedo by itself will interchange. We keep one of each in stock (used), so we can just slap it in when you need one. A lot of the problems with the clusters on these models is the connecter directly behind the speedo. You can easily remove speedo itself and tighten the connections on it. This fix is for the ones that the speedometer doesn't work. You know the kind you can slap the dash and they go to working.
Dan Tucker
transman@prodigy.net
Well I did not repair the VSS problem. I did wire the lockup ground directly to the 4th gear switch. Thanks to those that replied.
Dale Blake
dblake@telusplanet.net
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Problem / Fix: Can anyone tell me if there is a book or list of 700R4 transmission codes that will tell me what year and model the trans came from. I am dealing with trans that came out of unknown vehicles. I am just a home shop builder. I have done my own 700R4s but i would like to start setting up some for stock streetrod use. Any info would be greatly appreciated.
Whitley Tabor
dodge312@home.com
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Repair History: None
Work Completed: O/H s/k Converter
Summary: When lock up comes on at 30mph it comes on top of 2-3 shift and becomes very harsh.
Sometimes it comes on a 40 mph and it is fine.
Whatinputs is the computer using to tell it to go into lock up.
Thank you,
Len
Leonard Marucci
len@kwiknet.net
Leonard: Being an 89, this should have the auxillary valve body. If this is so, then with the pan off, you will see the wires that go to the lockup solenoid, temp switch, which is 2 prong and is just held on by a bolt) and a pressure switch (the connector going to the switch should be green). First off, you must remember that "most" domestic vehicles ALWAYS have 12V going to everything, which means that most electrical components are live and the computer either decides to ground this device or just be informed that the devise has grounded itself (circuit completed and devise is activated). Now since you are locking up, that means the computer is sending the 12v, so lets concentrate on the pressure switch. I'm at home and my computer recently crashed, so I do not have access to the hydraulic diagrams that I want. I am working from memory and cannot remember which gear activates the pressure switch. If you will send me a reminder after 9AM EST, I will receive it at my office and will be able to respond with a more accurate fix. Good Luck. Jim, III
Jim III
stardust@frontiernet.net
How is your throttle pressure? Might try increasing it.
Dell Wellons
woodchpr@worldnet.att.net
Hi Leo what I use to install I delayed lock up valve from G.M.these valve was for correct the problem on diesel units if you install the valve and gasoline applications is necesary to cut two o three coils of the spring is supply in the kit is all I remember for now good luck.
Willie Torija
wtori@prodigy.net
Hi Janice check to see if the valve body and gov. is not for a 6 cyl. this type of set up will cause a very early upshift specialy for 350 engine hope this can help.
Willie Torija
wtori@prodigy.net
After I road tested it a few times, the lock up went up to 40 mph. I delivered the vehicle.
Leonard Marucci
len@kwiknet.net
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Problem / Fix: Hi folks!
After installing a lot of TransGo kits I readed in the instructions on the last page of the full kit something about a road test sheet and 4 work sheets that should included in the kit.
Unfortunately I have had never a kit with this infos.
TransGo told me they canceled this infos because of nobody wants them.
Does anybody have this infos?
It would be very helpfull to have it.
Otherwise what are your recommend road test procedures on the 700?
Any help would be great.
Rosi germany
Falk Rossberg
falkrossberg@t-online.de
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Repair History: OH Unit 3 times and last time it got a purchased reman unit. Keeps coming back with same problem. Customer does not seem to abuse. He does light hauling (lawn mowers).
Work Completed: RB unit as outlined above
Summary: The fluid always seems to be full. We have an Aux Cooler and inline filter installed. We have never had this many repeat probs with a 700?? I was wondering if it is perhaps posible for the fluid to leak into the t-case and then back into the trans when sitting still causing the trans to RUN low on fluid but check ok. I know that sounds a little far fetched but I am grasping at straws here???
Joe Stewart
mjment@fuse.net
Joe If you haven't checked the tech tips or fix database at TRNi, then this would be a good time to do so. There are a lot of tips in there on this problem. Definately look at the input shaft seal of the transfer case, that year should be hard and brittle by now.
Don Oremus
dkoremus@execpc.com
Hi Joe- I've replaced a bunch of transfer case input seals on GM 4wd's, but I don't ever recall fluid leaking back into the tranny.It's always the other way..fluid leaks from trans.into transfer case. Do you have any pressure readings for us to go by? Cowbell
Joey Campbell
bccampbe@neocom.net
Joe: In my mind the worst customer that you can get are these guys that mow lawns in the summer and plow snow in the winter. If they do landscaping also, it is just a disaster waiting to happen. I get top buck from these people. Is your cooler being run separate from the radiator, if not please do this. Has the pressure regulator valve been modified by removing that one land for cooling. Always overfill this puppy by one inch on the stick. Lastly, they should be instructed to never, ever tow in OD. They always come into the shop pulling the little trailer and then one day you see them tooling down the road with that monster steamroller on it. Good Luck. Jim, III
Jim III
stardust@frontiernet.net
Joe- Don Oremus is right...if the transfer case seal has'nt been replaced already,it should be.Willing to bet it's hard as a rock.I just have'nt seen one cause the fluid to come back into the tranny before. Cowbell
Joey Campbell
bccampbe@neocom.net
Hi Joe one of the bigest problem this unit has is a leak on the third accum. check ball, also the travel of the pin for 2nd. and 4rth remenber only .062" to apply is only thing I can remember, hope this help .
Willie Torija
wtori@prodigy.net
Hi Joe, Everyone has given excellent advise so far. You must get a gauge on this. If there is ANY delay in pressure rise compared to throttle (it should be like you have a string attached to the gauge from the peddle), the clutches will start to go, beginning with the 3-4's. Make sure that the 3rd accum capsule isn't leaking and good bushings, endplay and rings are essential to help keep the oil from crossleaking into/out of the input housing clutch packs. If you are POSITIVE that all of these are good, the TransGo Jr. Shift Kit would help cure the common problems on these trannies.
Leo Schneggenburger
lschneg1@rochester.rr.com
check tv cable geometry , tv cable isnt hooked to an edelbrock carborator is it?
Donald Day
trnsmaster@home.com
Joe, My best advice on this unit is to check pressures. But if you already have it apart, than take and remove the 3-4 acc. check ball in the servo area and plug it with a 400 park pawl plug, than build up your input housing and plug your bottom hole in the input shaft and inject air through the check ball in the housing, should hold air for 15 seconds minimum, also if there is a bleed hole near the input shaft about 1 1/2 inch away (has a plug with about a .020 hole) plug it with a bb ( you can get one ofthese from your kid) Also when air checking make sure there is no leaks around the input shaft where it's pressed into the housing ( put brake cleaner around it) Use only Borg plates in the 3-4's ) If the capsule with the check ball in the housing leaks you can get new ones #24208262 from GM.
Steve Allbee
sallbee@worldnet.att.net
Joe, one last thing, make sure and install the .500 boost valve and the biggest cooler Trucool makes.
Steve Allbee
sallbee@worldnet.att.net
Hi Joe If I'm reading your post in repair history,you rebuilt the trans 3 times and then bought a reman unit.I would think it's external if that's the case.The only things I can think of would be make sure it does go into LU,not just commanded. And put some preassure on the radiator,pump it up good and see if you still got cooler flow.On the transfer seal I've only seen it go to the transfer,if so much oil goes to transfer that it would cause transfer problems it should blow out the transfer vent.I change the seal every trans overhaul and use the double lip single seal type.Oh also on the inline filter, pull it off and check the pipe,make sure the pipe was reamed after the cut,it may have a very small orfice now. Hope this helps,See Ya Harold
Harold Field
trblshtr@tdstelme.net
Pulled Unit back out and t-case front seal that was replaced twice(The double seal between the t-case and the unit) was as hard as a rock! We always change these things but I guess we got ahold of a bad one. Unit has obviously leaked into the t-case because the t-case was way overfull. The kicker is, the customer had a driver that had been adding atf and he did not tell us. So when we checked it and saw no leaks we assumed that is was not leaking. WRONG!! That was what was buring up the 3-4 clutches. He would run it low, fill it up and run it low again. Does not take long for the 3-4's to go in that scenario.
Joe Stewart
mjment@fuse.net
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Repair History: None
Work Completed: completely rebuilt transmission. new convertor
Summary: truck came in blowing out pump and vent. tore down found lock up solenoid bad. rebuilt transmission, new converter, new lock up solenoid. install all psi are good. test drove was all good locked up worked fine. release truck to customer. customer has 30' travel trailer hook up and got 7 miles down the freeway in 3rd gear with a 50 mph head wind and blew out the top vent. went to tow the truck back in and fluid was ok so I ask the customer to drive it back and no problems. unhooked trailer and test drove. everything is shifting great. what am I looking for to repair this problem.
Dennis Johnson
ace1@gorge.net
Dennis, put the biggest Tru-Cool transmission cooler that will fit in this puppy. Run it SEPARATE from the radiator. Be prepared to be amazed, you will drop around 100F of transmission operating temperature. Good Luck, Jim, III
Jim III
stardust@frontiernet.net
Hi Dennis, 50 mph head wind and 30 foot travel trailer? That spells a very hot condition for the transmission. I agree with Jim, III put the biggest Tru-Cooler on this thing. I imagine if it had a trans temp gauge it would scare the owner out of his wits. Good Luck,
Roger Pryor
whizwheel@aol.com
Hi Dennis, I couldn't agree more about using the TruCool LPD cooler but, you describe conditions where I'll bet the converter was not locked and therefore the cooler will not be enough. In extreme cases you may have to change other areas to make the trans live. What axle ratio does this have? You may have to lower it to keep the converter locked under those type of conditions. You will have to drive it with the trailer and see if it is staying locked under all conditions. Did you also grind the 2nd land on the PR valve? This will keep lube flowing if the converter is locked but the down side is that you lower the overall pressure when you do this. Although it won't help keep the unit locked under those conditions, you would be wise to install a TransGo Reprogramming Kit (too heavy of an application for just the SK)in this job to keep the frictions alive down the road. Make sure that the pump halves are flat, too.
Leo Schneggenburger
lschneg1@rochester.rr.com
D.J. What kind of trans fluid are you using? I have had this same problem and I corrected it with scyn, atf. I use Ansoil atf on all heavy duty and Chrys trans.
Robert Kauffman
fox2377@aol.com
Hi Dennis, I agree with the others bypass the radiator cooler, Tru-Cool makes a real nice large cooler 11x11x 11/2" I my opinion it is to heavy to mount to the radiator, use the straps that come with it and leave some room between the radiator and cooler, It works great. Also drill out the COOLER FEED HOLE IN THE PUMP TO .125 ( 1/8" ) I do this during every 700 rebuild, also grind off the #2 land of the pressure regulator valve and use the .500 ( 1/2" ) boost valve this will get the fluid flowing real good and keep that puppy from puking oil. Dave Foster d.b.a. The Transmission Technician 1312 Morningside, Dr. Melbourne, Fl. 32901 321-728-1155 AAMCO Master, A.T.R.A., & A.S.E. certified
David Foster
transtech@spacey.net
Hi Dennis- I am a little confused when you say "went to get truck,fluid O.K." Was the trans.full? If so,then is it possible that it may have been overfilled when it left the shop? I agree with JimIII that a large Tru-Cool aux.cooler should be installed...he's right about the drop in trans.temp. One other thing that I have noticed on most G.M.4X4 transfer cases is the input shaft seal is most always brittle after 75,000 mi.or so. That will let trans.fluid enter the transfer case,and many times cause the t.c.to leak from the vent,or will push out the plastic plug on the top. Hope this helps
Joey Campbell
bccampbe@neocom.net
Hi Dennis, had this problem and found thin o-ring in overrun clutch was torn. Hope this helps. DEL
Delbert Gray
delinpa@pa.net
Does truck have heavy duty trans cooler?If not this is very well could be your problem.Does fluid "foam up"?I have had this happen to me several times before and trans cooler fixed mine every time.Hope this helps.
Mark Hall
mark46martin@aol.com
Dennis, There's only a couple of things that'll cause this. The T/C airerating or a crossleak in the pump. Loose bushings in the stator support might cause it to aireate. And a crossleak in the pump will send pressurized oil right into the vent circuit. Follow the vent circuit through the case & into the pump. Look at the casting around the circuit. Are there any nicks? Or maybe it's just not flat. Since it doesn't do it cold or even at normal temps, an easy fix might be to thicken up the oil with some synthetic motor oil & install a cooler. Good Luck & let us know.
Ted Turney
tedeb@pacbell.net
WHAT SPEED ARE THEY GOING? ARE THEY TOWING IN OD OR 3(D) EARLY 700'S WOULD VENT WHEN TOWING IN OD BECAUSE THEY WOULD NOT HOLD IN LOCK-UP.
Thomas Baldwin
tb7ny@yahoo.com
Install Larger cooler corrected all problems
Dennis Johnson
ace1@gorge.net
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Problem / Fix: Wanted to say thanks to those who responded to my previous post on July 26.2000 for 700R4 trans identification codes. Recieved tremendous help from Mr. Glanzer in Illinois. My complements to TRNi for a great web site and to all those that post. You all are some of the most knowledgeable people that i have ever come across. Thanks again.
Whitley Tabor
dodge312@home.com
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Repair History: none
Work Completed: building trans
Summary: building a 700r4 for a 72 chevelle,customer does not want lock up,had a converter built with no clutch. is ther anything else that needs to be done in the trans when using a converter with no cluch?this is an early non aux. valvebody unit.anyone out ther do this before.i never built one with out a lockup cluch before and dont want any problems.using a 30,000lb cooler and ground the land off the pressure reg. valve.
Anthony Petti
sburnout@aol.com
Yes there is, but it's not a big deal. You have to put in a valve made by Transgo, in the pump where the lockup valve goes. And then take out the encapsilated checkball at the end of the input shaft, and leave the o-ring off. Of course I'm sure by now you realize you don't need the solenoid. :> Just make sure you use a good cooler.
Darwin Upton
darwank@usinternet.com
Anthony, When doing this, you must use a valve in the pump to replace the CC valve. TransGo makes it. Ask your supplier........... Emory
Don Emory
mwolfing@vicon.net
Ditto, transgo non lockup valve for pump reroutes converter & cooler flow correctly.
Bernard Robbins
gearbox@dellnet.com
Hi Anthony, ASlong with the TransGo L/U valve, make SURE that this car has low rear gears (min. 3.73, 4.11 is better).
Leo Schneggenburger
lschneg1@rochester.rr.com
thanks,used the transgo valve,worked fine!
Anthony Petti
sburnout@aol.com
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Problem / Fix: Installed new Bryco stator support and had 3rd gear starts and bind
up in manual low. The problem was a defective Bryco stator. There
is a crossleak between the forward clutch feed and the 3-4 clutch feed
underneath the pressed in steel sleeve in the stator due to poor
casting.
I called Bryco to inform them about the problem and at first they
seemed unaware of the problem and said they would check into it and
call me back, the next day after not hearing from them I called
again and was told that there was indeed a problem and explained
the casting flaw. He also said that they had 18 complaints about it.
I would suggest that everyone aircheck their stators before
installing them, I had 2 defective stators, one was purchased last
week and the other about a month ago from ATC-METRAN.
If Bryco had known about this they should at least notified us
or their distributers.
Tom Whitty
twhitty@nji.com
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Repair History: rebuilt transmission
Work Completed: visual
Summary: we have a diesel suburban that has had the wiring removed for the lock-up. My question is . If we grind the land on the pressure regulator valve can we run without convertor lockup?
and if not this is a 1982 vehicle so can we simply hook 12 volts to the connector on the transmission to have lock-up. We tried checkballing the solenoid but it really makes a pig out of it
thanks
David Duste
dustman@wave.net
David, Is there a reason you don't want it to work as it was designed?
Kenneth Hayes
deranger@ipa.net
David There is an inexpensive kit available from superior that will make a mechanical lock up. They work great. No wiring required. It comes with 5 different springs so that you can set the lockup at whatever speed you want. I just installed one yesterday and was extremely impressed. The vehicle shifted to od at 48mph anf then converter applied at 55mph. Its much easier than rewiring the vehicle.
Tommy Painter
county9@yahoo.com
Hi David, I would install the TransGo Shift Kit (full, not Jr). It will allow you to use the checkball setup, plus it will fix the horrible shift timing that the '82's had. It will also make the trans last a lot longer, too.
Leo Schneggenburger
lschneg1@rochester.rr.com
David, if this trans is an 82, than you should a lock-up shift valve train in the valve body. With this you can use a heavier spring to raise the speed at which the lockup clutch applies. If you make to late though, you may get a complaint of loss of fuel mileage seeing that this is a diesel. If you have a Transgo kit, they give you plenty of springs for this application. Bob Perry
Robert Perry
bobauto2000@aol.com
Dave: I agree with Leo & Bob. In addition to what they said, I would install the roll pin for the lockup valve train upside down from the bottom. That way, if you choose the wrong spring and the lockup speed is either still too early, or too late, you can change the spring with the valve body still in the truck. You won't have to remove the valve body. I just hate lubricating my eyeballs and armpits with hot ATF. :-( Sincerely,
Larry Bloodworth
larry_b@certifiedtrans.com
use normaly open switch 4th gear port in valve body nearest 2nd accm and run 12 volts to it 4th gear only lock up.
Les Richardson
lesauto@kca.net
Dont buy any shift kit save half the money and get the lock up valve from the dealer. Part # 08673299
Brian Rogers
eatons_trans@netzero.net
Dont buy any shift kit save half the money and get the lock up valve from the dealer. Part # 08673299 Brian Rogers eatons_trans@netzero.net Brian, Isn't 8673299 the number for the speed sensor(VSS)for the large hole extension housing?
Michael Habif
mhabif18@aol.com
The reason for not bringing it back to stock operation, is that the vehicle is a assembled mess. An old logger rig that has the wiring in a mess.
Sounds like the Superior kit is the ticket to eliminate the wiring. Have ordered one and will install tomorrow. Also has anyone put one in on a diesel and which spring from the kit did you use?
Dusty
David Duste
dustman@wave.net
Used the superior kit for eliminating the wiring and it worked great. Used the heaviest spring and it worked very well with the diesel. Thanks very much for all the info Dusty
David Duste
dustman@wave.net
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Repair History: pressures are as follows P,N,OD,3 w/o throttle 140 to 150 psi w/ full throttle 180 to 190 psi R 215 psi w/o TV R 270 psi w/ full TV 2 210 to 225 no matter about Tv 1 175 w/o Tv 1 215 w/ full Tv
Work Completed: Hello folks! I overhault this tranny w/ all recommendations and w/o any short cut. installed SK700 TransGo senior ,471" main boost valve 2nd boost ,3" rev boost ,37" line bias purple AND white spring (recommend by TransGo at phone) enlarged Tv balance hole to 0,062 (recommend by TransGo at phone) after press test removed plunger and sleeve and pressures are good (about 75 to 80) TV valve free to fall out due to it´s own weight plunger #94 Spacer gaskets correct pump slide free to move installed failsafe checkball back
Summary: Any idea on this would be great.
If some one answered it would be great to have a phone #
maybe there is a back question.
The customer needs his car ASAP.
Thanks to all in advance.
Rosi germany
Falk Rossberg
falkrossberg@t-online.de
Falk, Disconnect the t.v cable from throttle body and check pressure. If pressure drops to 80 +/- 10 psi then remove t.v. plunger spring and install original one and readjust from inside car not at throttle body. Good luck
Paul Moore
n8249b@chartertn.net
Hi Falk- This a just a shot,but is the t.v.cable link hooked to the t.v. bracket(in the pan)closer to the pan rail than to the v.b.?I seem to remember an old bulletin concerning this. Like I said,just a swag. Cowbell
Joey Campbell
bccampbe@neocom.net
Hi Rosi, Did it have the fail safe ball in it when you disassembled it? I have some of those that didn't have the little pin in the tv linkage to offseat the fail safe ball. Just a thought.
Roger Pryor
whizwheel@aol.com
Hi Falk, A couple of things come to mind. Normally, the TransGo SK would have you leave out the failsafe checkball, for this reason. Have you tried it without it? This would also allow you to try it with the TV cable disconnected just to check. If that doesn't do it, make sure that the TV Limit valve isn't sticking.
Leo Schneggenburger
lschneg1@rochester.rr.com
Falk is the cable bracket touching the tv plunger in the pan? I hope this helps Phillip
Phillip Gongre
bojaxx@aol.com
Hello folks!
Thanks for all the replies.
After removing the failsafe ball the pressures are fine.
PN43 w/o TV 80psi
PN43 w/ TV 165psi
R w/o TV 125psi
R w/ TV 250psi
2 225psi
1 215 psi
All shifts feeling good also good performance.
But it wouldn´t 2-1 kickdown.
The cable adjustment is tightest I can.
This mean the lightes touching the cable boost the pressure at the gauge.
Only one click more boost the press w/o any throttle.
Nevertheless there is no 2-1 kickdown.
The throttle cable linkage is the originally one from a "crossfire" TransAm of ´84.
What should be the total cable travel from zero to full throttle?
Anything else that could be important here?
Thanks in advance.
Rosi germany
Falk Rossberg
falkrossberg@t-online.de
Hi Falk, The correct range of travel is 1 7/8" from closed to WOT. If this isn't correct, fix this first. I have seen factory setups that didn't have the correct travel, especially on THM200's. Was that CrossFire a 700? Are you saying that the car won't WOT 2-1 after the minimum throttle 1-2 upshift, as the SK instructions tells you to check? Or is it that it doesn't kickdown 2-1 at a point that you feel it should? Make sure that the injector throttle plate is actually at the wide open position first and then, with the pan off, make sure that the plunger is fully seated in the VB at WOT. If that is OK, take the SK instructions and make sure that all of the end plugs are in place that go in the VB (the little aluminum plugs). Next make sure that the individual TV throttle valves for each shift valve is properly indexed. You will see a flat indentation on the end of each of the TV Valves that will line up with the roll pins when they are in correctly. Also make sure that any pressure switches that are on the VB don't leak when checked (some will squirt a little oil out as they are air checked, but it shouldn't keep blowing out). Is this the correct trans for the car or is it a transplant? If all parts, especially the VB and governor are original and these checks don't bring out the problem, you may have a factory mismatch of one of the VB components. At that point you may be better off contacting TransGo again with what you find but if you want to call me, my home number is 1-716-872-6505 and my work number is 1-716-288-9070 (5AM till ?), this is Eastern Standard Time here.
Leo Schneggenburger
lschneg1@rochester.rr.com
Hello folks! I double checked line bias, TV limit, PR, both boost valves. No mismatch, misassembly or sticking. I figured out after flooring the pedal w/ engine off and start it the pressure pumps up from 70 to 140 psi. Starting w/o flooring the pedal before give immediately high pressure. The failsafe ball can effect this as Leo mentioned. I removed it and got good pressures. After correcting the TV cable travel to 1 7/8" as Leo mentioned I have had a good road test. Thanks for all your ideas. Hopeful you have good day. Rosi germany .
Falk Rossberg
falkrossberg@t-online.de
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Problem / Fix:
Chuck-
You need to post to the "new transmission problem" area. We can't reply to a "problem/fix' post as it is a one time message.
To answer your question, there are different sized of feed holes in the reverse input drums and if you use a drum with the big feed hole
in a late tranny you will get a really harsh reverse engagement. Likewise, if you use the late drum with the small hole in an early
trans you will get a reverse delay. Just check the size of the hole and try and match it.
Kit
-----------
Kit Lindsay
Lindsay Transmission
1111 South Maguire
Warrensburg, Mo. 64093
www.lindsaytransmission.com
660 747 2272 You pay
800 875 4588 I pay
660 624 2861 Cell
660 747 2861 FAX
Serving on TRNi with the Industry's Best Shops
-------------------------------------------------------
Subject:
4L60E, Reverse input drum interchange - PROBLEM/FIX
Date:
Wed, 6 Sep 2000 13:49:12 -0700 (PDT)
From:
TRNi Inc
Mileage: 140000
Repair History: Just rebuild with a Gill Y. Jr shift kit
Work Completed: road test make sure up shift and detents are ok
Summary: Just rebuild with a Gill Y. Jr shift kit.
Everything works great.....except just before coming to a stop,
you can feel it down shift very noticeable. Any suggestion.
Question 1. Does anyone know why Gill Y. puts a special plastic check ball No. 5 in
the (bath tub location) in the valve body.
Question 2. What does it do?
Thanks
Walt
Leo Schneggenburger
Kim Walton
Falk Rossberg
Was only affected in D position only
The way I understood it from the Trans Go tech is that will happen in drive but not od
OD position works fine.
Walt's Trans
Mileage: 10600
Repair History: none
Work Completed: none pending
Summary: 700R-4
Subject:
Mechanical Diode by Raybestos (forward sprag replacement)
Has anyone installed one? If so what would be your rating
form 1-to-10 and any comments.
I would appreciate your input.
Walt
THANKS
Frank Choate
Richard Ennest
William Anthony
Darwin Upton
John Lovell
Ron Geddert
Stanley Roper
Decided not to use the manecanical dioe after reading the input
information from the rebuilders.
Walt's Trans
Mileage: 88000
Repair History: None
Never bin oh
Work Completed: Road test
Summary:
Transmission has never been worked on.
Can ay of the following be the cause?
Question:
1. TV cable adjustment
2. Fast engin idle.
3. Governor.
4. Band out of adjustment
5. Can a broken accumulator Spring the problem?
Your input will be appreciated!!
Walt
Falk Rossberg
Frank Choate
Walt's Trans
Larry Bloodworth
Was only affected in D position only
The way I understood it from the Trans Go tech is that will happen in drive but not od
OD position works fine.
Walt's Trans
Repair History: Rebuilt a year ago.
Work Completed: Check main line and testdrive. 1-2 TOO early at 5mph at light acc..Other shift right on time.Adjust tv no change.Main line as follow:
Warm at idle : 65psi in d4,d3 and120 in d1. Reverse is 115.Pressure rise is good.
Summary: Is there any way too correct 1-2 shift. I did have .283 int./rev and
and.471boost valve.Thank you.
Hello Quan , put a heavier spring on the 1-2 shift valve it should take care of your problem.
Curt Preston
Hi Quan,
I would check your 1-2 shift valve spring. Could be broken or weak.
Daniel Wills
Quan,
There are truck 700s that are calibrated to shift
early on the 1\2 and regular shift on the 2\3 and 3\4.
If that is not to your taste the replace the valve body
Stuart
Stuart Kay
Thanks everyone, i removed the valve body this afternoon and the 1-2 shift vakve spring was broken in to two pieces.I Stole another spring from a stock valve body, and it worked great.Thank you once again. Quan in Texas.
Quan Trinh
Repair History: unknown
Work Completed: Transmission was burnt up. Rebuilt transmission,install one of dacco pump and torque converter.also install ball and capsule.flushed system good. After installing transmission back in vehicle it cuts the engine off in forward and reverse and also has fluid coming out of the overflow.
Summary: Have anyone out there had any problem like this other than a 4x4 that's listed in the fixdata. The torque converter was replaced on the second installation after the first attempt. Could it be in the rebuilt pump from dacco? Dacco pumps comes with out the valves in them. Check all valves when pulled out the first time and all was free. Any suggestion other than putting it out of it's misery.
Try this: Remove the cooler line, out to cooler, put a fitting and a hose onto that fitting at the case and run the hose into the filler tube. Then try it and see if you have the same problem. Slowly pull the hose up out of the filler tube and check flow.
I'm guessing that you have a resticted cooler or cooler feed and the lack of cooler flow is backing up inside the converter and applying the converter clutch.
Also something to watch for on rebuilt pumps is missing cup plugs.
Jimmy Taylor
This is probably not much help but........
A couple of years back we had a pump from Dacco that was missing some of the small cup plugS.After we put an experianced pump in all was fine.
Timmy
Timothy Carney
Pull it out and check the face clearance of the pump. You prabably have a bad pump. I quite buying Dacco a long time ago because of these kinds of problems.
Gerald Martire
cooler flowed fine for about 30 seconds and then started releasing air.
after all the headache we finally put another dacco pump in and that took care of all the problem.
Janice Easter
Repair History: got bench job after another guy rebuilt 3or4 times, we believe he switched valve bodies,after install late 2-3. increased governor waits and better but still needs to come down to 30mph from 37. switched 2-3 valve train and sleeve to larger diameter from.459 to .479 with little effect, but left spring the same.
Work Completed: switched 2-3 valve and sleeve to larger diameter from .459 to .479
Summary: we have been told that the seperator plate is diffrent for a diesel. identification? we are going to try a softer sring next in the 2-3 assy.but the one we have is only slightly softer and i thingk the larger diameter valve and sleeve we installed would have had a more pronounced effect than a spring change. tips, suggestions? this is our first use of this service
Sam:
You need diesel valve body, transfer plate, regulator valve train and governor. Usually, when you run into these differences it is because someone replaced the diesel engine with gas, and the transmission shifts too soon. Yours is the opposite.
As far as the transfer plate goes, you need GM part # 8654483, which has the letter 'S' stamped on it.
HTH
Lane Floria
Hi Sam
You say it's your first time on the net here,well welcome,it is
a good tool.I think your going to need to get a deisel VB and plate,
and maybe govenor,Transtar can help you with parts.
Hope this helps you,See Ya
Harold
Harold Field
HAD THE SAME PROBLEM ON A PICK UP TRUCK.THE VALVE BODY&SEPERATOR PLATE IS DIFFERENT FOR DIESEL APPLICATION.
Don Harrington
ended up changing only seperator plate with a "b" diesel seperator plate with little effect. changed 2-3 shift spring to a lighter working height. we thought that changing the valve and sleeve from a .459 to .479 would have a greater effect since a bigger diameter increases the pressure at the spring but it seemed to have less effect than changing the spring itself. alls good.
Sam Jones
Repair History: trans was rebuilt a few yrs back came in with 2-4 band smoked and 3-4 clutches wasted everything else ok
Work Completed: after pan removal pulled unit and did a oh mok,band,tc,sk,etc.
Summary: on road test found l.u. was coming on right after 1-2 shift we disconnected lu. outside trans and adjusted tv cable works great customer had to take truck was going camping this weekend will bring it back on tues. or wed for diagnosis its been so long since i had this problem on one of these i forgot procedure on checking for this problem. this vb. has 3 switches on it can someone tell me most common things to check on this thanks in advance.
Greg: I had a 4T60E do the similiar think once and I had left a small thimble filter out of the channel plate, found out this was a orfice restrictor, install it and worked fine. But what going through my minds eye is I can't recall that type of an orfice in a 700 except for the govn. feed at the rear of the case and the lock-up filter in the front of the case. If that front filter is left out could this be the same problem?
Frank Nelson
Sounds like one of the switches is stuck on. The lockup solenoid is energized all the time.
Dale Blake
hi Gregory
700's use 2nd gear oil for l.u. & some lu on top of 2nd / release shift to 3rd /lu, release / 4th then lu again
sometimes hard to get around on some models.
does yours have a tcc valve in v.b.assy' if so replace it w/ a stronger spring that won't coil bind etc. in sleeve / or use desiel set up .
might cut "d" wire wire in series w/ non grd s/w in 4th tap/servo if two wire type
just be sure not to put ball in snout of sol. seen this cause same complaint on some models.
Frank Wadlow
Try unplugging the LU wires from the case. If it still has LU you have a Hyd problem
Jeffery Funk
You know since you unpluged the trans & problem stopped I would be looking for a short to ground on the negative side of the solenoid harness, because there is 12v power to the solenoid with ignition on & brake released. Maybe the insulation is cracking on the wires in the pan & shorting against a wire clip, or heavon forbid an r&r man pinched the harness in the bell housing, if not then the ground wires run up the driver side back of the motor to a vacuum switch mounter on the firewall between the brake booster & the engine. Hope this helps.
Bernard Robbins
Greg, if I'm not mistaken the unit you are working on should have a tcc valvetrain. The unit always has a hot coming from the computer on the earlier models,the switches just pull to ground. True you probasbly have a bad switch but I would try to recalibrate the tcc circuit with another spring also. Should'nt lock up that early even if the switch was hung in that year model........ Tommy
Tommy Bolton
closing thread
Gregory Gaal
Repair History: trans exchanged with shelf unit
Work Completed: trans exchanged with shelf unit
Summary: We have hooked up signal monitor (uncertain if it was hooked up correct) We hooked the positive red (Popper tester) to the red on lock up solenoid and the negative black to the ground side of solenoid. Light does not come on at all.
Any help would be greatly appreciated.
Hi Christopher, key on engine off there should be 12 volts to tcc solenoid red wire this voltage will go away when stepping on the brake, if thats good then its up to the computer to ground the solenoid depending on tps & vss & map inputs. Or you can attach the tcc ground wire to a normally open 4th gear switch & tcc will come on & off with 4th gear.
Bernard Robbins
Christopher,
Check the "F" terminal on the DCL under the dash. If the "F" terminal isn't B+ then check the brake light switch and the computer.
Good luck.
Roger Pryor
We replaced a circuit board enclosed in a black box next to the module. The fuse on the board was burned out. (sorry but I do not have part numbers).
Christopher Helmuth
Repair History: This is a rebuilt core off my self,with SK,OH kit,convertor.I
do bushings etc and get piston travel down in paks.I'm thinking
it must be related to the two symtoms but don't see it.
Work Completed: All shifts except 2/3 are good and on time.No kick down but cable is free and adjusted.,VB on bench now but don't see anything to cause this that I know.
Summary: I have air checked it and all sounds right as far as bleed by and piston travel.I air checked servo and that moves good.All
the valves are moving,so if you can point me in the right direction I could use it.
Thanks
I hope I'm not considered a bone head and am filtered off all your e-mails
See Ya
Harold
Hello Harold,
My first inclination is a poor pressure rise problem. I'd make sure that your cable is adjusted properly first of all. Second, I'd put a gauge on it and check for good pressure rise. This step may uncover your problem right away. Make sure you don't have a worn out boost valve. Personally, I put a .500" boost valve in all 700's. They are readily available from Sonnax. This would especially be a good idea in a hard working 4X4. Luckily for you, you can do this without pulling the trans out. It's a bit of a hassle getting it back in, but it can be done.
If this is not your problem, then you may have a problem with the checkball capsule in the case leaking. The one that's directly behind the band servo. Normally, I pull all of those out and put a cup plug in it's place. It definitely won't leak and I've never had a problem doing this.
If that still is not your problem, you may want to check your servo. Do not EVER use a 554 servo. In this truck, I probably would have gone with a 092 servo if it's a V-8. If it's a V-6, I'd go with a 553. The servo not only applies the intermediate band, but also acts as the accumulator for 3rd gear. If the servo is too small for your application, you can get a flare.
The last thing, which would be aweful, is too much clutch clearance in the 3-4 clutches. Personally I prefer to keep mine pretty tight. I usually keep it around .030" Too loose could cause a flare. Also, you may want to check your band clearance. I like to keep it at .125" of travel. If it's too much travel, you could always weld on the end of the servo pin to get the desired travel. That's all I can think of for now.
By the way, you are not considered a bonehead. Just be sure to post a good fix so we can all learn from each other. Also try and help your fellow transmission brothers when they are in a pinch. That's what the whole thing's about.
Fernando Rosales
Transmission Physicians
5802 S. Dale Mabry
Tampa, Fl 33611
(813)835-8728
Fernando Rosales
October 02, 2000
Hi Harold,
No...you're not a bonehead and don't even consider it! With regards to your 700 with 2-3 flair and no K/D, the two symptoms seems to fall into the area of insuffcient pressure rise.
Since you didn't post any pressure readings, it's difficult to pinpoint the cause. Install the TV lineup into the VB. Look carefully at the middle lands on the TV valve through the round hole in the VB casting.
Now depress the TV plunger to the bottom. When the plunger is fully depressed, the two lands on the TV valve must be visible towards the 9:00 position in the VB casting hole. Ensure that you have this valve and all others free and properly installed.
Install the VB and before you put the pan on, have someone step on the throttle to the floor and ensure that the TV plunger is bottoming. Put the pan on and install a gauge. Test drive and if the 2-3 flair and / or no KD is still present, record the pressures (especially during the 2-3 flair) and update your message. Stevie L. TEST Research.
TEST Research_Tech_Dept
Hi Harold-
Is it possible that you have a mis-match on the v.b./separator
plate? (vented line bias valve vs. non-vented type.)
Just the first thing that popped into mind.
This maybe a "bonehead" reply! :-)
Cowbell
Joey Campbell
Check the throttle valve, and make sure there is no extra spring on the inner most valve. I have had several come in where a previous builder has added a return spring similar to those we use on the Chrysler governors, to the throttle valve. These springs cock and cause problems with the tv system.
Gerald Martire
Harold,
Double and triple check your valve body gaskets to make sure that you are using the right gaskets for this unit.
Been there done that, causes wierd problems.
Gerald Martire
Thanks for all the replys,I just got back to the garage and still
have the VB on bench.I didn't start with oil psi because I was sure it was in the kick down area,I had installed SK and thought I messed it up.So I checked all the valves,plate,and gaskets,and all seems well.I tried to get the plate down without loosing the balls so I could see if I messed up there,too late now for oil psi so I'll get there after I get it back together.I always air check clutches on bench and check the hub etc and unless I was sleeping that all should be ok.Pak clutch gaps are always set down around .030 or as needed,I never skip that,again unless I was sleeping,but still you can hear nice clutch apply.I am going to pull servo to see if something is messed up there.Travel is always checked on bench as well as capsule.
I'll get back with fix(positive thinkging)or oil psi which ever is needed.
Thanks for the help,I am always looking for something I can help you all with,but most of what I've done is the older stuff,and you've all been there.This is the first time I've ever had this problem,I don't have problems often but when I do I am weak in fixing them.
See Ya
Harold
Harold Field
Oh I forgot to mention on the earlier post I'm not sure if you call it flare what this is doing.All shifts are good and on time and rev is good,one reason I skipped oil psi and went strait to no where.It shifts to 3rd at right time,you feel the timing of the shift then nothing then it's in 3rd,so maybe it is something other then flre.
Harold
Harold Field
Harold, just change the entire input sprag assembly. Put in the one that you cannot see the copper ring as you look down into the input housing. I have been fooled by a few of them, so if you already have the second design, then replace with same. Good Luck Jim, III
Jim III
Hello again
Well I got VB on and same thing.I am hampered by the lift kit he's got on the trk.I cannot get it in any gears lower then OD,on the colum.It starts in low and shifts up ok.The oil psi's for P=80/150for R=120/225,N=80/150and OD=80/150,I was on road and when the flare happens oil psi's stay at 80 as they are when you take off and it goes 1-2.I did have kick down some at lower end.I would like to see oil psi in manuel 1-2&3 but colum will not go down,He's at the end of rod.The servo looked good,I did find some fussy material from rags
in it and cleaned it out.I guess I'll have to take it out.
See Ya
Harold
Harold Field
Well Fellars it's working OK.I can not tell you the fix.I had unhooked the shift rod and put it in first by hand to test further and out of frustration I floored it because his rear brakes aren't worth two cents and the wheels spin instead of getting stall After the hand shifting for oil psi's I went for one last run before I took it out and it shifts great and has kickdown.Go figure.I use the thick paper out of kits on my bench surface and once I caught a peice of it in one of the pump capsules and luckily I saw it before I but the pump in.Somewhere looking in Transdoc and the CD I see something about pump capsules,so I don't know if when I floored it maybe something blew out.He's going to take it and I'll hold my breath.
Thanks for all the replys and help.
See Ya
Harold
Harold Field
Repair History: Rebuilt Trans Kit, Band, Input sprag, Converter, Shift Kit
Work Completed: Pulled Trans 2-4 Band Cooked All Clutches Looked Fine
Summary: Is This A Servo Problem I Have Tried Two Used Servos Thanks
Hi John,
Could you provide us with more detailed info, starting with pressure readings? This is all ranges at: idle, fast idle, and fast idle W/TV pulled full, plus, how is the TV response (does it respond as if the gas peddle is attached to the gauge so that whenever the peddle is moved, the gauge should move). Was the band 'cooked' originally? Is this an actual Shift Kit? Does it have the original carb setup (meaning is the TV geometry correct)? How is the 1-2 accum piston and bore? What size servo are you using (should be a 553, minimum and never the 554)? You can also put a gauge on the 2nd and 4th oil, to see if you are getting oil in the curcuit at the wrong time, dragging the band.
Leo Schneggenburger
hi john, things to look for, bad drum not straight check with a straight edge, weak spring in back of servo use blue spring from superior,install s-kit, also check checkball capsule in case inside servo hope this helps.
Gregory Gaal
Hi John, Leo makes a few good points, is the carb a rochester & does the arm bottom out the plunger at WOT with the pan off? Who's shift kit, did it tighten up band clearance (can help a warped drum, straight edge across band surface), 553 & two groove pin, change to a 3 groove pin & a 093 servo, 1-2 accumulator piston to pin fit, check it with the 3-4 pin from case if it wobbles change it, if the housing is scratched up change it or install sonnax fix.Needs a good sound pump 2 slide springs for more pump volume, .500 boost valve & green PR spring for good line rise.1-2 feed hole size depends on taste, I like it smooth & firm 093piston-.95, 553-.110. I'll assume you didn't change the case,spacer plate, or valvebody, so you shouldn't have a mismatch, but your kit should help you there.
Bernard Robbins
After pulling this trans four times we removed the retainer & ball in the servo and pluged that hole. We put the trans back in and had a good second gear, but after about six or seven miles lost second but still have forth. Pressure is park & neutral is 63 psi reverce 105 psi d4 63 psi d3 63 psi d2 & d1 120 psi we have tried 3 servos where do we go from hear THANKS.
Sound like your going to have to pull the trans back out, this time use a borg band and make sure the travel of the band is only 1/8. Oh and check the reverse input drum with a straight edge.
Steve Allbee
Hello John , 256k thats alot of miles . I didnt see any main line pressure readings so I will guess . check the boost valve if thats ok , go to your 1-2 accumulator valve it is either worn out or the spring is dead . sonnax makes a service kit for this and it comes with 3 springs to dial it in . hope this helps
Curt Preston
Hi John, I had this same experience once only on a 700, good forth and no second, after many attempts to solve the problem we finally determined that the case bore in the area where the outer seal for the second clutch piston rides was worn. We made a seal by using a servo straight cut seal from something but I do't remember what, sorry but it worked fine and stayed out. It's something to check. Good Luck!
Hal Quantz
If it worked fine for a little while, maybe your servo cup plug started leaking.And you know I worked for GM thru the '80's & chrysler & olds thru the '90's & have built more 700's than I can remember & have yet to ever need to change or delete the servo check ball. Reading some post it seems alot of guys do.
Bernard Robbins
Hi John,
I am reposting my original response in hopes that it will be answered:
Could you provide us with more detailed info, starting with pressure readings? This is all ranges at: idle, fast idle, and fast idle W/TV pulled full, plus, how is the TV response (does it respond as if the gas peddle is attached to the gauge so that whenever the peddle is moved, the gauge should move). Was the band 'cooked' originally? Is this an actual Shift Kit? Does it have the original carb setup (meaning is the TV geometry correct)? How is the 1-2 accum piston and bore? What size servo are you using (should be a 553, minimum and never the 554)? You can also put a gauge on the 2nd and 4th oil, to see if you are getting oil in the curcuit at the wrong time, dragging the band.
I see that some pressure readings were given but the rest must have been cut off somehow from your post. Also, What does the cup plug have to do with second gear? It is on the 3rd gear side of the servo. If that helped then you must REALLY have a problem.
Leo Schneggenburger
Somebody said to chk the band clearance and from experience that is what I would do first. I had one do the exact same thing after I machined a little too much off of my reverse drum. I had no 2nd but I still had 4 th. You can bet that I chk the travel on the band regularly now ,especially when I machine the drums. Tommy
Tommy Bolton
Hi, John. If the band was originally burned from the first rebuild, I would try a shorter length servo pin or grind the pin that you have a few thousanths so your band will be a little looser. Might try to sand the reverse input drum and check with straight edge. Good luck, Jason.
Jason Gilbreth
Thanks for all your help. It was the Reverce Input Drum where the band runs wase not flat. I never had this problem before, But I will check it from know own. Thanks again
John Sines
Problem / Fix: Car runs till hot then goes neutal noisy, sounds like stripped sun shell.Cant find problem inside.Is not in transfer.
Repair History: Rebuilt after convertor failed
Work Completed: Installed check ball in lockup solenoid as customer claimed he had intermitent no lockup
Summary: Trans had failed torque convertor, did complete overhaul, now customer says there is no engine braking when slowing below 70 km (40 mph) on a grade the car coasts away & he has to ride the brakes, also swears that lockup came on in 2nd before we overhauled it. We did not alter any calibration on the valve body (no shift kit). Lockup occurrs at 65 km (35 mph), vehicle has engine braking in manual 2nd & low.
Hi Ken, it's possible that it did have lockup in 2nd before, but GM didn't desiegn it too. It's should come on in 3rd at about 30-35 mph with lite throttle. no engine braking in drive range would be a leak in the coast clutch circuit, the reason it comes on in manual 2nd & 1st is the increased line pressure in these ranges overcomes the leak.
Bernard Robbins
Ken: First off, get that check ball out of the solenoid. If you have a M200 Sk laying around put the RED accumulator spring in the TCC valve. This weighs in at 11 pounds, you can go up to 16 pounds. This will put you into LU at a higher speed. It will also kick you out of LU at a slower speed. As far as 2nd gear LU goes, that is just stupid. I like to have it come on right after 4th, but that would take some wiring changes. I will be glad to help with this. I recommend that you do the spring change first. Get that check ball out. Remember the solenoid can be charged, but if the TCC valve is not stroked, then no LU. Good Luck and please post the fix. Jim, III
Jim III
Vehicle never returned so I,m closing this thread.
Ken Buehler
Repair History: rebuilt trans complete
Work Completed: basic test
Summary: need wiring diagram for tcc. this is a calif. emissions and is a bit different. ecm will not ground the sol. but I can't find out which wire from the ecm is to test. could use a diagram real bad. thanks Jeff
Hi Jeff,
I don't have the schematic but how about making it L/U hydraulically by blocking the sol snout with a checkball?
Leo Schneggenburger
Jeff:
What Leo says can possibly help. I've personally done it many times. However, if it does fix it, when you deliver the vehicle to the customer warn them of the 'trailer-hitching' effect. When you perform this modification, the TCC doesn't disengage when you let up off the gas. Also, lockup can come in slightly early and give the driver the feeling of "no power" or "lugging the motor".
For several years I was using the diesel poppet-valve converters in these to avoid the 'trailer-hitching' effect, but the cores for these types of converters have become very rare. Almost extinct.
When they went to the 30-spline input shaft in '87; that idea didn't work unless you had a custom built converter. :-(
Sincerely,
Larry Bloodworth
Hi Jeff
Your FAX number please...........
--
-----------
Kit Lindsay
Lindsay Transmission
1111 South Maguire
Warrensburg, Mo. 64093
www.lindsaytransmission.com
660 747 2272 You pay
800 875 4588 I pay
660 624 2861 Cell
660 747 2861 FAX
Serving on TRNi with the Industry's Best Shops
-------------------------------------------------------
Kit Lindsay
thanks for the responses, I had the customer on my back and wound up tracing the wiring. was a pain in the butt, but it had to be done now, you know what I mean. Thanks any way. Jeff
Jeff Anglesey
Repair History: scan for codes none presant
Work Completed: All seems to be fine with this vehical however vehical is extremely over loaded wont stay locked up cause you have to keep your foot at least half throttle to maintain speed 55mph
Summary: Is there anything I can do to satisfy this guy converter is constansly locking and unlocking tps voltage is about 2.00 volts when it unlocks and this is where he has to keep the throttle to maintain speed.
Well it's an '87 model, so the VB should still have the hole for the lockup valve train. Install the late lockup valve train & put a ball in the solenoid & lockup will come on around 4th gear & unlock with kickdown pressure. Of cpurse if it still kicks out at the speed he wants to drive, install the early sleeve & valve & spring. This will bring it on around 35 mph & be much harder to kick out. If its got that much weight on it, without torque mutiplication from an UNLOCKED torque converter it probably wont maintain speed unless even more throttle is added. He should have bought a heavy duty 3\4 ton instead of the light duty 3\4 ton & he would have an axle ratio made to tow & a 4l80e instead of a 700. Although I don't remember GM making the light duty 3\4 ton untill about '90. Anyway, if its working that hard, you better get a big cooler on it.
Bernard Robbins
Jody: Have roger install a 16# coilbind spring in the TCC valve. Jim, III
Jim III
Your post does not mention whether or not it is unlocking in 4th or 3rd. Assuming it is 4th and it is very overloaded, what happens when the owner puts it in 3rd? Whenever we get a customer that trys to do things with a vehicle that it was never suppose to do, we take them for a special test drive. With the vehicle in 4th at a 55 mph cruise, manually downshift the vehicle to 3rd without changing your accelerator position. In most cases, the vehicle will gain speed and you will find that you have to let up on the throttle to maintain your cruising speed. End result is more power with better fuel economy. Dave Schaffel dbschaffel@home.com
David Schaffel
Jody, Let's see the 1987 model is computer controlled TCC. This means that the valve body should NOT have a TCC valve in the valve body, but a plug instead. It should have a 2 wire TCC solenoid. It should also have a a 4th gear and maybe a 3rd gear switch. The gear switches do indeed affect the TCC command strategy. A bad 3rd or 4th gear PSI switch can cause 'ticky' TCC apply and release. What you need to know is the TCC being commanded to release? Look at the gear switch state positions on the scanner while driving it. 2.00 volts is close to being so heavy of a throttle, that you may have to alter the vehicle in some way to offset the load.
Dan Tucker
This is a Jasper unit under warranty and after contacting there tech guys they want us to replace the lockup sol. Customer has taken vehical and we ordered new solenoid awaiting customer to return vehical for work to be completed. Will keep you all posted of actual fix.
Closing this thread we replaced tcc solenoid as per request of Jasper engines and transmissions. This job has been extremely difficult in determining the customers complaint even when driving down the road with this customer his complaint changes everytime he is questioned never get the same story twice. We observed the lock up not releasing when applying the brake or letting off the gas brake switch is working. Customer wired up his own computer we are passing the buck on this one.
Jody Schroeder
Repair History: overhauled unit last year. always had flare. unit works perfect otherwise.
Work Completed: changed fluid and filter.
Summary: is there any fixes without r&r. i have the valve body on the bench. thanks for any input.
Hi Jacob,
Were there any tricks done, like hogging out the 2-3 feed? IOf so then resize the hole and try it again. Otherwise you can try tightening the band adjust and see if it helps. If not, the TransGo Shift Kit should take care of it.
Leo Schneggenburger
The old gil kits sometimes created this problem. Quick and sleazy repair is to go one size bigger on the servo piston. If you shift kit the superior works better for this problem. Don
Don Callender
this trans does have a gil kit. 3rd feed hole .170. 3-4 accumulater has stock natural spring. sorry for leaving this out.
Jacob,
The 3-4 accumulator does not affect 3rd gear. Only 4th. I normally just block that one off by ramming a checkball into the case.
As far as your 3rd gear flare. Just step up to a Corvette servo and that should take care of it. It will firm up your 1-2, but it will also firm up your 2-3 and most likely remove the flare. The servo acts as the 3rd gear accumulator.
Most importantly, I think you should have checked your pressure. If you have too low pressure, you can get the flare and putting in a bigger servo will only mask a deeper problem. You should definitely check the servo size. 554 is absolutely unacceptable. 553 is Ok for V-8's, but I prefer the Corvette for heavy use applications.
Fern
Fernando Rosales
HI Jacob,
Is this the Reprogramming Kit or is it a Shift Kit? That .170 feed sounds like the problem.
Leo Schneggenburger
Jake, The easiest way to cure a 2/3 flare,is a sonnax #77701-076. Its a check valve assembly, that cures 2/3 shift timing when the feed orfice has been drilled out. Ernie
Ernest Spear
Never go more than.125 on the feed hole. Could be your problem. Restrict down or change sep plate. Put the strongest spring you've got in the 1-2 accum. Block the 3-4 accum. You can use an old piston on top of the new piston or an old GM speedo gear. Try it You'll like it. Don
Don Callender
I have to agree with Leo on this one. I would say that .170 is way to big.
Bob Perry
Robert Perry
REPLACED SEPERATOR PLATE AND FLARE IS GONE. THANKS EVERYONE FOR ALL THE INPUT.
Jacob Holdrege
Repair History: t/c changed 6 mths ago by dealer for a l/up shudder
Work Completed: i o/hauled unit and changed input drum( just to be on the safe side) couldn't see too much wrong inside other than the 3-4,s were a little burnt.customer didn't want t/c changed
Summary: I dont believe this is l/up related because tapping brake pedal the l/up applies perfect.
If you didn't change the converter, is your TV contaminated and sticking?
Don Callender
What kind of crunch? Is it fresh or stale,your not giving us much help.
Fred Whitaker
Sorry guys for the short description, but I had the customer breathing down my neck. To fill you in, what i am experiencing sounds like a metallic shudder on the 2-3 shift and also will do it on 3-2 forced downshift. Its hard to get it to do it every time. Truck must be hot and will do it regardless of where t.v. cable is set.I disconnected lock/up to rule that out and still does it. It will only do it on lighter upshifts if you put your boot into it it works fine. I hope that helps, thanks for now.
Andrew, Check the inner sealing ring on the servo (the large one)
for shrinkage.Take it off and fit it into the servo bore.I had
some make a metallic chatter noise on the 2-3 and the 3-2 shift
from a batch sealing rings that shrunk.
Gerry Gallus
Dont know if I fixed or not but havent heard from customer. I changed the input sprag and sanded the races, also polished the 2-4 servo pin as it had some marks on it. Thanks for the help, Andy.
Andrew Faulkes
Repair History: Vehicle came in with burned up 3/4 clutches.
Work Completed: Tore down and installed overhaul kit, rebuilt convertor, flushed cooler lines. Did not install shift kit or do any other modification.
Summary: This truck has good line pressure at idle and good line rise-all within spec. Shifts ar good and not delayed. But no up shift to 4th. Used a tapped 2-4 servo cover to pressure guage-no pressure.
Removed governor and valve free and no slop in bore. Used another 700 R-4 governor-still no pressure at 4th servo. Went through the fix feed backs and used vacuum hose to wddge out the governor weights and its starts in 4th fine and has good pressure and line rise (this was done on the rack). I am not sure what the next logical step is. I am assuming the 3-4 shift valve had to stroke to get 4th. I even pulled the valve body again and checked it over carefully for sticky/stuck valves-none were that way-all free. I am stumped on this one although someone I am sure has the obvious answer.
Thanks in advance,
Respecifully submitted,
Loren Knighton
Woodland, CA.
Loren: We have a TRNi member (Ron Widing) whom I'm positive will respond to your problem. He is the inventor of a transmission program called TransDoc. Ron is evidently on drugs, because he sells this program too cheap. Strongly recommend that you consider this as an addition to any other shop diagnostic programs that you may have.
I never begin a teardown without it. It allows me to instantly focus on just about any problem. So, sit tight Ron will be with you shortly. Good Luck, Jim, III
Jim III
Hi Loren,
Check the pressure switches on the VB. Often they will leak causing this problem.
Leo Schneggenburger
Loren,
You say you're checking this in the rack. Do you have no 4th on the rack or have you driven it and have no 4th. We have run a few on the rack and couldn't get 4th. When we drove it, we had 4th. Don't know why and not all of them are like this, only a very few.
Dell Wellons
Sounds like a leak in the front pump. We air check pump on bench for cross leakage. Saw one that one of the encapsulated check balls fell out of stator. Had several that leaked line at the boost valve. Try the sonnax boost valve 1/2 inch id. They all will cause a loss of line and never make enough pressure to take 4th. RPM kits have a bulletin to drill a hole in the sep plate to cure 3-4 clutch burnup. DON'T do this. causes same problem. Take two cross leaks and call me in the morning. Don
Don Callender
Well this one is down the road shifting fine. I am very grateful to all that took of their time to lend suggestions and Ron Widing to Email the list of his Trouble Shooting Guide 9. Went through everything on the list. Still no 4th. Then I remembered Dell Wellons said he had a few that wouldn't get 4th on the rack but on the highway they would. So I took this beast out in the country and it shifted fine. Never had one like that before. I don't get it but at least it's ok. Also thanks to Jim 111, Leo, and Don Callender for their help. This was my first post and a happy ending.
Respectifully submitted,
Loren Knighton
Woodland, CA.
Loren Knighton
Repair History: o/h transmission with new reman pump clutches seals
Work Completed: reinstalled line pressure was at fifty in park, falls off to 0 when you drop in gear and graually rises then falls back off gets lower when it gets hot, tried differant valve body no change
Summary: has anybody had a problem with pump that looks real good or should i look elsewhere
Paul did you put the thimble filter in the pump? Reman units don't come with that or the big ball and spring for pressure relief. Good luck, Don
Don Callender
thanks for the reply Don. never did see anything wrong with visible portion of pump, but ended up replacing it with another reman after pressures were fine.
Paul Egleston
Repair History: Morning sickness. Oh unit and replaced the TC
Work Completed: extended breather tube and installed cooler
Summary: Customer states that vehicle interm. blows atf out the vent. Any solutions. Trans works great. Thanks
Richard: If you are not running the cooler separate from the radiator, then please do so. If the problem continues after that, then you have a warped pump. Good Luck. Jim, III
Jim III
Another thing that will cause that smae problem is wrong pump gasket. You need the one that covers the baffle on the pump. Good luck, Yogi
Jeff White
replaced the fr. pump
Richard McClain
Repair History: None
Work Completed: none
Summary: I would like to Know if anyone has install a V-8 in a S-10 and what modifications should be done to trans, The motor will be a TBI engine, All computor working, I want trans to shift smoothly like stock, Not going to be pulling heavy loads. Any info About Transmission would be helpful. Thank You
No Response. Oh Well Trial and Error
Gary Nelson
Mileage: 165882
Repair History: rblt 4yrs ago, this is second time back in last 2 years; truck is lifted with 34"tires, speedo is accurate,shift points are good for ratio. At first doesn't want to go to OD, once in it feels bindy. Last road test lasted 3 miles, 1mile in od, coast clutches welded together, went fwd all gears. Only coast clutches burnt, checked input drum, was bleeding across into coast piston when 3-4 clutches were applied. Replaced drum with earlier drum, used shaft from original trans. same, problem not as bad?
Work Completed: see above.
Summary: What should we do to verify where problem is? (v.b.;drum,case?)
Leo Schneggenburger
Mark Pugliese
William Anthony
Billy Tippit
George Whittaker
The author's membership with TRNi expired. Therefor, the thread was closed with no fix.
Repair History: None
Work Completed: Teardown for inspection
Summary: Hey guys....Got this one tore appart and cant see anything wrong. Frictions look new. No valves stuck in vb, no cracks in any pistons, no hard parts damaged. In reverse, it feels like parking brake is on. It will back up if you rev engine to about 2500rpm, but as soon as you let off gas it stops like the brakes are on. All forward gears are okay. Checked both front and rear brakes and the drums and rotors roll free backwards. Read the fix database and didnt see anything there. Anyone have any ideas?
Hi Tommy,
I seem to have a vague recollection of a problem in the aux. VB causing this. However I don't remember exactly what. Might be worth a try to just swap it out.
Clayton Allen
Do you have any other info. Was this a recent rebuild? or did this just happen all of a sudden.
First check check ball locations if it is a recent rebuild. If it happened all of a suden look for something that may cause something to apply or hold while low/rev clutch is on with rev input clutch.
Good luck
Paul
Paul Moore
Tom,I can remember I had a simular problem, turned out to be a real long valvebody bolt in wrong location binding on the shell,hope this helps.....joe
Joe Zahn
What's it do in forward ranges?
Don Callender
4-3 sequence valve or 2-3 shift valve stuck in uipshifted position (ATSG # 89-67).
Possibly too long VB bolt, 2nd from front, 2nd row from shift lever side, binding the shell, but that would give you a 2nd gear start and a 2-4 shift.
Gary Glaenzer
Tommy, is this a 700 or a 4l60E? If it is a 700 with an aux. valve body, make sure that you did not install the checkball in the bathtub in the main valve body. Correct me if I am wrong, but the long bolt only applies to the 4l60E.
Bob Perry
Robert Perry
It happened all of the sudden. This trany had never been apart before. I haven't put it back together because I couldn't see anything wrong. All forward gears appear to be okay. No stuck valves or blown gaskets. No hard part damage. No scorched or burn clutches. Everything looks perfect.
Tommy Painter
Had the same happen to me, used a new pump without any valves in new pump, installed new TCC and PR valve and installed and had same problem, torn down trans and everything looked good except looked at pump and forgot to put in the spring and large ball on side of pump, everthing worked fine, did you change out pumps by any chance.
Frank Garlick
This is usually the 4-3 sequence/ 3-4 relay valve lineup that causes this. It is the band being applied causing the bind. Put the car on the lift and pry in on the servo cover and have someone put car in reverse. If cover pushes out then I'd look at this valve real close. Have found that valve won't be stuck, but will have something causing it not to CLOSE all the way. Had a couple that on bench looked fine, pulled valves out and found sliver of metal laying in bottom of passage. HTH
James
James Northum
WE cant have A bind up without toasting clutches.I,d look at them emergency brake cables again.
Fred Whitaker
Tommy, it sounds like we have a checkball in the wrong place. CJ of Canada
CJ of-Canada
Found a small aluminum shaving inside the 2-3 shift valve aluminum capsule. The valve was free, but when pressurized, that small piece of aluminum filing would hang that darned valve. As soon as you shut engine off and removed valve body...valve was free. Would never have found it you guys not told me to remove the valve and look for cutting inside capsule. Excellent diagnosis. You guys are great!!!!
Tommy Painter
Repair History: Overhauled:
New Clutches,Band,Seals,Gaskets,Corvette Servo,.500 Boost Valve, New Input Sprag, & Rebuilt Converter.
Work Completed: Still here from overhaul.
Summary: Flares on kickdown after 60 mph. Kickdown fine from 3-2, 2-1, and even 4-3 between 50 -60 mph. After 60 mph when you kick it down, it flares up then catches and goes. We did pull it again and seen nothing wrong. Went back through everthing. Even tried another sprag. Still again same problem. Let me know what else it could be. Thanks
Hi Mark,
Did you sand the races when you had the sprag out? If the races are still polished, the sprag can 'hydroplane' until the oil film goes away and then grab. Was the reverse drum and/or the sunshell flared out when you first did the job? If so, then this is a classic sign of a major slip/grab of the sprag.
Leo Schneggenburger
Repalced Vavle body and Spacer plate. Someone had wrong setup intstalled. Thanks for all the help.
Mark Bowler
Repair History: none
Work Completed: rebuilt trans with a supirior shift kit .
trans has a delayed engagment in reverse and slips then grabs.
the stator had a small diameter feed hole and the reverse drum had a large square hole with the steel piston.
i then replaced the boost valve to a size 4.72 and the inter. valve and rev. boost valve to a 2.80 size , but with no results.
the reverse drum had no leaks upon pressure testing it , the low revese clucth pack also had no leaks .
i had replaced the pump also but with the same casting numebers.
the idle on the engine is around 600 rpms is this enough rpms for revers?
forwrd engagment is ok with no delay , thier is a slight flare on the 2-3 shift , even with the larger boost setups.
Summary: could this be a valve body problem ?
or a pump problem ?
thanks in advance
frank
Frank,
Do a pressure test in all ranges at idle and wot for 1 sec.
Look for boost in reverse. Could be cut seals, incorrect clutch stackup, worn valves, many things!!
Paul Moore
Hi Frank
What pressure do you have? If it is idling at 600, why don't you put a coin or something between the
throttle stop and the linkage to get the idle to 700-750 and then see how it engages. We have dealt with
this same problem a couple times and it was idle related in our case both times. I am sorry I don't remember
what we did to increase the idle though. It has been a while but someone on the net here may
know a shortcut. Hope this helps-
Kit Lindsay
Frank, you changed the pump. Does it have the thimble filter and the ball and spring in the stator side. Seen both of those left out on lots or reman pumps. Don
Don Callender
hi everyone , i want to thank everyone for there replys .
the fix was the revese drum had to much clearance.
asfo the 2-3 flare , installed a corvett servo.
frank
Frank Islas
Repair History: none
Work Completed: overhaul,kit and clutchs.input drum,bearings,converter,new stator,s/k shift kit.
Summary: trans air checks all clutches in input drum,3/4 applies through pump.but i still dont have 4th gear.checked everything in book this morning.and cant see the forest for the trees.help has anyone run into this before.thanks in advance for any help.kyle
Kyle,
The 3-4 clutches stay applied in both 3rd and 4th. If you have a good and solid 3rd gear then the 3-4 clutch is not the problem. The servo applies differently for 2nd and 4th. For 4th gear, the pressure is directed to the piston that is in the servo cover. A torn or missing teflon ring in that location could cause your concern of no 3-4. Seeing as you stated that the 2-3 shift is stacked, my money would be on sticking valves in the valve body. The 3-4 shift valve likes to stick a little after a rebuild sometimes. Also, over-torquing the valve body bolts could cause them to bind in the bore too.
As to the 2-3 shift, I am assuming that you mean it shifts 2-3 shortly after the 1-2 shift. If so, that could be caused by a broken spring in the 2-3 shift valve line up. I hope this helps!
Robert Bruce
Have you taken a good look at the Gov ? When you check the Gov remember when checking the movement of the inner weights that the very last small drop in the valve is your 3-4 shift. High mileage units will wear the weights & pins & prevent the 3-4 shift. Try a diifer gov with the same size weights.
Jeffery Funk
sorry i forgot this one its been so long ago,but put new v/b gaskets in and all worked well.thanks kyle
Kyle Tuttle
Repair History: Vehicle originally had a 350c that has failed. The transmission has a spacer that when removed, allows a 700 to fit without changing driveshaft length so a swap seems logical now as per the owner.
Work Completed: Finishing the overhaul as we speak
Summary: I have a 700 2-3 kit and I was wondering what the brown checkball is for. Transgo's lines are real busy at the moment
brown ball goes in valve body.......in the bathtub portion..it is in the instructions...goodluck....brian reagan
Brian Reagan
Carl. The brown check ball is I think the #9 checkball. It goes in the valvebody, there is a bathtub back towards the park pawl. It was eliminated on 1988 and later models and some 1987 models. Check your separater plate if it has 2 round holes, it takes the checkball.
What year of a transmission are you installing?
The reason you have a block between the 350c and transfer case is because somebody had already converted the truck from a 700r-4 to a 350c. You are putting it back to original.
Dale Blake
I too remember the 700 kits,
It seems to me that the larger checkball was to put into the
tcc solenoid so the kit could take control of lock up.
I know it was this way in the earlier kits. I have not usd a kit
in probably 9 years. So it may have changed.
Yogi
Jeff White
You can go to the bank with this. The 5/16" checkball is for the TC solenoid spout (Don't do it) The big plastic ball is for the bathtub at the rear of the VB. The early units check ball was enlarging the hole in the separator plate, that's the reason for this oversized ball.
Good Luck. Jim, III
Jim III
Members submitted excellent info and vehicle is as good as done
Carl Wassermann
Repair History: none
Work Completed: none
Summary:
got a toyota truck, friend of mine, he put a 12 inch lift kit on it and put a chevy drivetrane in it. interestewd on the best way to hook up the lock up.easy hard i dont know. hes always doing weird stuff.
Tony,
Superior makes a really simple kit to eliminate the wiring on these units and still have lock-up. Part # 5107. It works as ling as there is a lock-up shift valve in the valve body (pre 1989 i believe)
David Duste
Tony,
If the unit does not have a 4'th gear pressure switch, I would suggest adding one that closes with 4'th gear oil. Run the lockup solenoid hot wire thru the switch to the trans connector. Supply power from a normally closed contact on the brake switch if that is available, if not available then run a wire from the brake lights to relay coil the other side of the coil to ground. Run power from a source that is on with the ignition to a normally closed contact, the other side of that contact to the tranny. This will give you lockup in 4'th gear, that cancels when you put on the brake.
Jerry
Gerald Martire
Eliminate the tcc. I do it myself but transco makes a kit, and put in a no clutch converter. He will be happier in the long run. Don
Don Callender
put a ball in lu sol in pump locks in 4th
Tony Yurkevicius
Repair History: Removed dead diesel and fitted 3.8ltr GM V6 with 700R4
Customer Complaint: No lockup.
Codes Present: No codes
Work Completed: All wiring is factory GM loom. Speedo has VSS reading through Tech 1. All inputs meet requirements as per GM manual. Speedo reading on dash differs from VSS reading but not enough to worry about. Lockup is not commanded even when put in overheat mode.
Summary: Lockup works if grounded at diag terminals and off ECU. Have changed ECU's and memcal. Memcal is correct for engine and trans combination. TCC is always commanded off. Temp, TPS, VSS are all correct on Tech 1. Someone else did this conversion and handed it to me. One of his friends has also done the same conversion by himself with the same result. Are there any other inputs that control lockup on this transmission.
Richard,
How about a MAP sensor? Diesels don't have a MAP sensor. Did you put one on the 3.8?
Dell Wellons
Richard:
First off, it's too late to tell you not to create a "Frankenstein" vehicle because it will come back to haunt you.
-HOWEVER-
To answer your question, TransGo makes a Shift Kit that will completely eliminate the need for electrical lockup. They put a checkball in the snout of the L/U solenoid and give you various springs to control when L/U occurs. When everything is right, it feels like a 5-speed.
It does this:
1-2
2-3
L/U (feels like a shift)
3-4
Richard, I've had customers come back and tell me they feel like I gave them an "extra gear" because of the fact L/U didn't happen right on top of a shift.
Try it, you'll like it.
Sincerely,
Larry Bloodworth
Richard....
Superior also makes a kit for hydraulic lock up instead of electric. Its fairly cheap and comes with several springs to adjust lock up speed. Its not a shift kit though, but it installs quickly and works great. I use them all the time and am very impressed with the way they work. Just for the record, I always use the strongest spring that comes in the kit. Trany usually lock up between 45 & 55 depending on rear end ratio. Try it---u will like it.
Tommy Painter
Richard, your ecu must be looking for some input that is not seeing and thus not allowing lock-up to happen.Depending on what year trans you are working with, the Transgo shift will fix this. But you need to have a lock-up valve train in the valve body to use the feature of putting the checkball in the snout of the solenoid. If you don't have that vblve train, lock-up will occur right on top of the 2-3 shift, feels like a double bump type and your customer will not like it. There are also some aftermarket devices that work very well, some that are even adjustable from the drivers seat so you set when you want lock-up to engage.
Bob Perry
Robert Perry
Richard
Does the scanner show if the computer knows it is shifting into high gear? Maybe a pressure switch in trans is not there or is bad, computer may not know that it needs to lockup.
Don Oremus
Hi guy's thanks for the input. I probably wasn't to clear on my origional post due to the half empty bottle of stress relief sitting next to me. The engine and trans swap is out of a Holden Commodore. That is just a rear wheel drive V6 and 700R4. Every sensor, wire and connector is accounted for. They basically removed out of one car and into the 4x4. It is a very neat conversion and not a disaster. I could cheat and use the hydraulic kit but I would like to get this right as it should be. (keeps me away from the wife). The vehicle drives really well. No vibes, cluncks or bangs. It drives better than a real V6 Navara ute. (couldn't think what it was called last night). I will keep on working on it over the weekend. Happy New Year guy's.
the lock up is also controled by the brake light switch if the power is not routed throug there acording to the wirering dig from the doner car and ran the same in the host the converter will not lock up
this is the power wire that powers the converter hope this helps
Milton Pierce
Richard if you dont want to buy any thing and you have some older valve bodies around, get a 3rd or 4th gear switch that is normally open "usually silver" and put it in either hole you want lock up to come in at.Cut the ground wire close to the case connecter inside the pan,run this wire to one of the two female spades on youre switch with a female spade. put another spade on a short piece of wire and ground it to a valve body bolt and hook it to the other spade.If you touch the brake you still lose lock-up and depending on which switch you use when you slow down enough to downshift from 4th or 3rd you disengage lock-up.
James Carter
1 hour of uninterupted diagnosis made the difference. Going through the tech 1 data in park while warming up the engine I noticed the inhibitor switch said it was in gear. I moved the lever through the ranges and it still said R-D-L. Checked the loom and backprobed ECU. Momentarily grounded terminal and tech 1 went P-N and then back to R-D-L. Without turning off the engine test drove and had lockup. Turned off and restarted had no lockup. While driving I momentarily grounded terminal again and we had lockup. Stripped wiring and found where auto electrician had snipped, tucked and taped it. Ran this to inhibitor switch and everybody's happy. Looks like the ECU needs to see a change in state on the input after each start.
Richard Keown
Kit Lindsay
lindsay2@sprintmail.com







QUESTION:
Date: Sat Feb 26 14:33:06 PST 2000
Subject: 700R4, down shift very noticeable
Vehicle: 1982 Chev 2wd pu 350
Walt's Trans
waltg@relia.net
RESPONSES;
Subject: 700R4, down shift very noticeable
Hi Walt,
I would grind the servo piston down in the center @ 1/8" or so. If I remember correctly they don't have you do that on the JR(or am I thinking of the 4L60E SK?). I believe that the rubber ball is meant to seal off the little notch in the hole on all but the diesel units to help keep the L/R alive. Personally, whenever I have an older 700 like that I use the full SK since it fixes all of the timing problems that they have. Maybe that is part of your problem?
lschneg1@rochester.rr.com
Subject: 700R4, down shift very noticeable
Hi Walt, I agree with Leo in the early 700's run the full Gil kit(NoYoYo)it fixes alot of shift timing problems.I fit the jnr to 88 up tran's only(with aux v/boby).There was a post yesterday about 700 (early)with lock up problems and the noyoyo was the fix.Goodluck!
Regards Kim
citytrans@webscene.com.au
Subject: 700R4, down shift very noticeable
Hello Walt!
I´m with Leo in the recommendation to install the full kit in the trannys before 1985 because of very common timing problems.
But I did not believe that the full kit will cure your problem if the Jr. can´t.
Was this complaint present before installing the Jr.?
I know there was an service bulletin for a complaint such as this. And you should grind the servo as Leo indicated. This will effect the 4-3 downshift.
Which down shift is your´s.
A time ago I have had a Blazer with a 3,73 axle from ´88 with the same complaint.
So I did not believe it´s a problem of early units.
But the customer didn`t like spend money in this. So I couldn´t find out it.
Do you have also an axle similar to this?
The 2-1 down shift is only releaseing the band by the servo return spring.
This means the L/R roller comes on. If this is too hard I fear you must live with it.
Good luck.
Rosi germany
falkrossberg@t-online.de
FIX;
Date: Thu Sep 7 21:04:18 PDT 2000
Subject: 700R4, down shift very noticeable
waltg@relia.net
QUESTION:
Date: Wed May 3 19:47:32 PDT 2000
Subject: 700R4, pending, OH
Vehicle: 83 chev pickup 350
Walt's Trans
waltg@relia.net
RESPONSES;
Subject: 700R4, pending, OH Subject:
I have never used one, have a friend that uses them exclusively, rates it a 10.
jfranklinc@aol.com
Subject: 700R4, pending, OH Subject:
Walt I have used one of these one way diodes with no problems so far
but after found out that they have a high failure ratio. I'm still
sweating on this one. Hope this helps.
rennest@cgocable.net
Subject: 700R4, pending, OH Subject:
I will not use them in anything but a drag strip trans.
Raybestos still does not have all of the KINKS worked out of this part.
The problem is when the transmission is in 4th gear the sprag or diode is overrunning. This causes the flappers of the diode to melt down or have premature wear because of the internal alignment of the rotating parts in the transmission.
(not everyone puts a full set of bushings in on every trans.)
This is what a Raybestos Tech. told me as well.
roadmaster.trans@att.net
Subject: 700R4, pending, OH Subject:
Yes,,,,,,I have used 2 of them,,,,,,,,,,,,and have had 2 CB's because of them. The problem is the outer "hub" makes contact with the inner race and makes metal,,,,,,lots of metal. When I had my failures, I talked with a Tech at Raybestos. He said they were in the process of redesigning the part,,,,,,possibly putting a bushing in there. They paid me for the parts and labor,,,even a TC. It was originaly made for dragracing. On a street vehicle, driving in OD, that hub is overrunning, and that is where the problem starts.
Soooooo,,,,, if you're intenet on using one, make sure they have updated it. I haven't checked into them lately, so maybe the problem has been solved by now. Call Raybestos and find out.
darwank@usinternet.com
Subject: 700R4, pending, OH Subject:
Hi Walt, I have used a couple. The first one took a crap. Raybestos did send me a check to cover the price of the diode and R&R. The other is still out there some where.
ent@crosslink.net
Subject: 700R4, pending, OH Subject:
Walt, we installed 3 of them about 3 or 4 yrs ago.Pulled them
all back out. my rating number is not on your scale
dadstran@home.com
Subject: 700R4, pending, OH Subject:
Raybestos removed them from the shelf. Saying that
they would not hold.
roper@nwol.net
FIX;
Date: Thu Sep 7 21:12:58 PDT 2000
Subject: 700R4, pending, OH
waltg@relia.net
QUESTION:
Date: Fri Mar 31 20:07:12 PST 2000
Subject: 700R4, Hard down shift
Vehicle: 1988 Chev p/u 350
Walt's Trans
waltg@relia.net
RESPONSES;
Subject: 700R4, Hard down shift
Hello Walt!
Do you mean coast down shift or half throttle or detent or with the selector?
Wich downshift or all?
The causes will be different.
Good luck!
Rosi
Falk - Mobile germany
falkrossberg@t-online.de
Subject: 700R4, Hard down shift
I think everybody on TRNi should get together when talking about downshifts, Lets specify, coastdown shift or kickdown shifts. I'm ASS-U-ME-ing since you mentioned engine idle, we are talking about a coastdown. Lets talk about what happens on a coastdown on a 700, in the OD selector position, a 4-3, 3-2, or 2-1 should not be felt if the engine idle is proper as it is overruning 2 sprags. At or after stop, it may jerk as the engine torques back into the forward clutch for several reasons, engine idle too high, bad mount, slack in the output shaft splines, slack in differential, bad U-joint, etc. In the D3 selector position, everything being normal, a very slight bump can be felt on a 3-2 coastdown and this is normal as the overrun clutch is applied, but not on a 2-1 as it is still overrunning the low sprag. On a kickdown, you'll have to be very specific, as to which gear, etc. Clear as mud?, I thought so.
jfranklinc@aol.com UPDATE:
Date: Sat Apr 1 05:08:30 PST 2000
Subject: 700R4, Hard down shift
Hard down shift (lack of information:)
Down shift can be felt while coming to a stop. Throttle closed trans in OD
waltg@relia.net MORE RESPONSES:
Subject: 700R4, Hard down shift
Walt:
An excessively fast engine idle can cause a harsh downshift on this year and make. Beleive it, or not, we had one come in that had a harsh downshift due to a bad thermostat. The ECM never saw the engine come up to temperature, so the natural fast idle the engine is supposed to have when cold, was always there. Customer replaced the thermostat....fixed.
However, if it was TV cable-related, you would have late & harsh upshifts, as well. I wouldn't think it was a broken accumulator spring (although they have a tendency to break a lot), or you would have a very firm 1-2 upshift.
Check the engine idle speed, first (because that's the easiest) and let the group know if it's in the 700 RPM range, first...then get back to us.
Thanks for the question, as well as posting you fixes. We can ALL use the information. Thank you. :-)
larry_b@certifiedtrans.com
FIX;
Date: Thu Sep 7 21:15:11 PDT 2000
Subject: 700R4, Hard down shift
waltg@relia.net
QUESTION:
Date: Wed Sep 13 09:45:49 PDT 2000
Subject: 700R4, 1-2shift too early
Vehicle: 1990 chevrolet suburban, 350
Mileage: 158000
Quan Trinh
qtrinh4805@aol.com
RESPONSES:
Subject: RE: 700R4, 1-2shift too early
gbat2@webtv.net
Subject: RE: 700R4, 1-2shift too early
danwills@mindspring.com
Subject: RE: 700R4, 1-2shift too early
powerflo@juno.com
FIX:
Date: Wed Sep 13 16:53:47 PDT 2000
Subject: 700R4, 1-2shift too early
qtrinh4805@aol.com







QUESTION:
Date: Wed Sep 13 19:10:23 PDT 2000
Subject: 700R4, oil overflow/shuts engine off
Vehicle: 1987 chevy caprice, 307
Mileage: unknown
Janice Easter
hun6@juno.com
RESPONSES:
Subject: RE: 700R4, oil overflow/shuts engine off
odie@gci.net
Subject: RE: 700R4, oil overflow/shuts engine off
timjames@prodigy.net
Subject: RE: 700R4, oil overflow/shuts engine off
transmission_doctor@yahoo.comUPDATE:
Date: Thu Sep 14 07:01:09 PDT 2000
Subject:
Janice Easter
hun6@juno.com
MORE RESPONSES:
FIX:
Date: Thu Sep 14 14:29:16 PDT 2000
Subject: 700R4, oil overflow/shuts engine off
hun6@juno.com







QUESTION:
Date: Thu Sep 21 09:16:55 PDT 2000
Subject: 700R4, late 2-3shift, 1-2good,3-4 not bad
Vehicle: 1986 chevy suburban, 6.5diesel
Mileage: gazillion
Sam Jones
transmission.exchange@imsday.com
RESPONSES:
Subject: RE: 700R4, late 2-3shift, 1-2good,3-4 not bad
lane@net-link.net
Subject: RE: 700R4, late 2-3shift, 1-2good,3-4 not bad
trblshtr@tdstelme.net
Subject: RE: 700R4, late 2-3shift, 1-2good,3-4 not bad
donhd53@sprint.ca
FIX:
Date: Thu Sep 21 15:38:54 PDT 2000
Subject: 700R4, late 2-3shift, 1-2good,3-4 not bad
transmission.exchange@imsday.com







QUESTION:
Date: Sat Aug 12 09:18:50 PDT 2000
Subject: 700R4, lu comes in right after 1-2 shift
Vehicle: 1984 chevy suburban 2 wd, 5.7
Mileage: 95,000
Gregory Gaal
gregg505@aol.com
RESPONSES:
Subject: RE: 700R4, lu comes in right after 1-2 shift
nelsonfj@wcoil.com
Subject: RE: 700R4, lu comes in right after 1-2 shift
dblake@telusplanet.net
Subject: RE: 700R4, lu comes in right after 1-2 shift
ftwadlow@aol.com
Subject: RE: 700R4, lu comes in right after 1-2 shift
shiftkit@specialtytrans.com
Subject: RE: 700R4, lu comes in right after 1-2 shift
gearboxr@home.com
Subject: RE: 700R4, lu comes in right after 1-2 shift
vegagt74@aol.com
FIX:
Date: Mon Sep 25 20:21:06 PDT 2000
Subject: 700R4, lu comes in right after 1-2 shift
gregg505@aol.com







QUESTION:
Date: Wed Aug 9 19:22:17 PDT 2000
Subject: 700R4, no lock up
Vehicle: 1991 CHEVY 2500 2wd Pick Up, 5.7 L V8
Mileage: 85000
Christopher Helmuth
transmissionhouse@hotmail.com
RESPONSES:
Subject: RE: 700R4, no lock up
gearbox@dellnet.com
Subject: RE: 700R4, no lock up
whizwheel@aol.com
FIX:
Date: Sat Sep 30 09:05:49 PDT 2000
Subject: 700R4, no lock up
transmissionhouse@hotmail.com







QUESTION:
Date: Mon Oct 2 08:08:29 PDT 2000
Subject: 700R4, No kick down/ 2/3 flare
Vehicle: 88 Chev PU 4x4, 5.7
Mileage: 150000
Harold Field
trblshtr@tdstelme.net
RESPONSES:
Subject: RE: 700R4, No kick down/ 2/3 flare
surflobstr@aol.com
Subject: RE: 700R4, No kick down/ 2/3 flare
testResearch@ibm.net
Subject: RE: 700R4, No kick down/ 2/3 flare
bccampbe@neocom.net
Subject: RE: 700R4, No kick down/ 2/3 flare
transmission_doctor@yahoo.com
Subject: RE: 700R4, No kick down/ 2/3 flare
transmission_doctor@yahoo.com
Subject: RE: 700R4, No kick down/ 2/3 flare
trblshtr@tdstelme.net
Subject: RE: 700R4, No kick down/ 2/3 flare
trblshtr@tdstelme.net
Subject: RE: 700R4, No kick down/ 2/3 flare
stardust@frontiernet.net
Subject: RE: 700R4, No kick down/ 2/3 flare
trblshtr@tdstelme.net
FIX:
Date: Mon Oct 2 15:08:23 PDT 2000
Subject: 700R4, No kick down/ 2/3 flare
trblshtr@tdstelme.net







QUESTION:
Date: Fri Aug 25 08:45:29 PDT 2000
Subject: 700R4, Soft 1-2 Shift
Vehicle: 1985 GMC JIMMY, 350
Mileage: 256124
John Sines
johnbsines@compuserve.com
RESPONSES:
Subject: RE: 700R4, Soft 1-2 Shift
lschneg1@rochester.rr.com
Subject: RE: 700R4, Soft 1-2 Shift
gregg505@aol.com
Subject: RE: 700R4, Soft 1-2 Shift
gearboxr@home.comUPDATE:
Date: Mon Aug 28 07:34:24 PDT 2000
Subject:
John Sines
johnbsines@compuserve.com
MORE RESPONSES:
Subject: RE: 700R4, Soft 1-2 Shift
sallbee@worldnet.att.net
Subject: RE: 700R4, Soft 1-2 Shift
gbat2@webtv.net
Subject: RE: 700R4, Soft 1-2 Shift
halq@hotpop.com
Subject: RE: 700R4, Soft 1-2 Shift
gearboxr@home.com
Subject: RE: 700R4, Soft 1-2 Shift
lschneg1@rochester.rr.com
Subject: RE: 700R4, Soft 1-2 Shift
vegagt74@aol.com
Subject: RE: 700R4, Soft 1-2 Shift
gilbreth@aeneas.net
FIX:
Date: Sun Oct 8 08:39:23 PDT 2000
Subject: 700R4, Soft 1-2 Shift
johnbsines@compuserve.com







PROBLEM / FIX:
Date: Sat Oct 21 06:08:15 PDT 2000
Subject: 700R4, Very noisey neutral after warm up.
Vehicle: 1988 Blazer s-10 4x4
Randall Fredette
caref@ctel.net







QUESTION:
Date: Wed Aug 16 19:55:23 PDT 2000
Subject: 700R4, No engine braking in drive position
Vehicle: 1985 GM Corvette, 5.7l
Mileage: 163,000 km
Ken Buehler
kbuehler@freespace.net
RESPONSES:
Subject: RE: 700R4, No engine braking in drive position
gearboxr@home.com
Subject: RE: 700R4, No engine braking in drive position
stardust@frontiernet.net
FIX:
Date: Sat Oct 28 20:41:58 PDT 2000
Subject: 700R4, No engine braking in drive position
kbuehler@freespace.net







QUESTION:
Date: Wed Nov 1 19:17:59 PST 2000
Subject: 700R4, tcc electric
Vehicle: 86 chev blazer full size, 350
Mileage: 80,000
Jeff Anglesey
apautooldtimer57@aol.com
RESPONSES:
Subject: RE: 700R4, tcc electric
lschneg1@rochester.rr.com
Subject: RE: 700R4, tcc electric
larry_b@certifiedtrans.com
Subject: RE: 700R4, tcc electric
lindsay2@sprintmail.com
FIX:
Date: Fri Nov 3 17:30:57 PST 2000
Subject: 700R4, tcc electric
apautooldtimer57@aol.com







QUESTION:
Date: Fri Oct 13 10:10:21 PDT 2000
Subject: 700R4, Torque converter wont stay locked up
Vehicle: 87 Chevy c20, 350
Mileage: 214000
Jody Schroeder
jody@compfxnet.com
RESPONSES:
Subject: RE: 700R4, Torque converter wont stay locked up
gearboxr@home.com
Subject: RE: 700R4, Torque converter wont stay locked up
stardust@frontiernet.net
Subject: RE: 700R4, Torque converter wont stay locked up
dbschaffel@home.com
Subject: RE: 700R4, Torque converter wont stay locked up
transman@prodigy.netUPDATE:
Date: Fri Oct 27 12:14:25 PDT 2000
Subject:
Jody Schroeder
jody@compfxnet.com
MORE RESPONSES:
FIX:
Date: Thu Nov 9 11:00:59 PST 2000
Subject: 700R4, Torque converter wont stay locked up
jody@compfxnet.com







QUESTION:
Date: Wed Nov 8 14:15:58 PST 2000
Subject: 700R4, 2-3 flare up
Vehicle: 1988 chevy k1500 p/u, 350
Mileage: 135
Jacob Holdrege
jakesrepair@aol.com
RESPONSES:
Subject: RE: 700R4, 2-3 flare up
lschneg1@rochester.rr.com
Subject: RE: 700R4, 2-3 flare up
tranclin@firstworld.netUPDATE:
Date: Wed Nov 8 18:53:14 PST 2000
Subject:
Jacob Holdrege
jakesrepair@aol.com
MORE RESPONSES:
Subject: RE: 700R4, 2-3 flare up
surflobstr@aol.com
Subject: RE: 700R4, 2-3 flare up
lschneg1@rochester.rr.com
Subject: RE: 700R4, 2-3 flare up
etranz49@gte.net
Subject: RE: 700R4, 2-3 flare up
tranclin@firstworld.net
Subject: RE: 700R4, 2-3 flare up
bobauto2000@aol.com
FIX:
Date: Thu Nov 9 14:24:27 PST 2000
Subject: 700R4, 2-3 flare up
jakesrepair@aol.com







QUESTION:
Date: Tue Nov 7 14:05:45 PST 2000
Subject: 700R4, crunch on 2-3 shift (intermittent)
Vehicle: 1992 chev p/up 1500 4x4, 350
Mileage: 254000
Andrew Faulkes
scutrans@aol.com
RESPONSES:
Subject: RE: 700R4, crunch on 2-3 shift (intermittent)
tranclin@firstworld.net
Subject: RE: 700R4, crunch on 2-3 shift (intermittent)
fwhit84684@aol.comUPDATE:
Date: Wed Nov 8 09:38:04 PST 2000
Subject:
Andrew Faulkes
scutrans@aol.com
MORE RESPONSES:
Subject: RE: 700R4, crunch on 2-3 shift (intermittent)
tsirichfield@mindspring.com
FIX:
Date: Mon Nov 13 09:58:50 PST 2000
Subject: 700R4, crunch on 2-3 shift (intermittent)
scutrans@aol.com







QUESTION:
Date: Tue Nov 14 22:25:39 PST 2000
Subject: 700R4, No 4th unless Gov. weights wedged out
Vehicle: 1988 Chevrolet Suburban, 350
Mileage: 157,000
Loren Knighton
backncardr@aol.com
RESPONSES:
Subject: RE: 700R4, No 4th unless Gov. weights wedged out
stardust@frontiernet.net
Subject: RE: 700R4, No 4th unless Gov. weights wedged out
lschneg1@rochester.rr.com
Subject: RE: 700R4, No 4th unless Gov. weights wedged out
woodchpr@worldnet.att.net
Subject: RE: 700R4, No 4th unless Gov. weights wedged out
tranclin@firstworld.net
FIX:
Date: Wed Nov 15 13:16:22 PST 2000
Subject: 700R4, No 4th unless Gov. weights wedged out
backncardr@aol.com







QUESTION:
Date: Fri Nov 10 17:14:51 PST 2000
Subject: 700R4, loss of line pressure
Vehicle: 1986 chevy suburban, 5.7
Mileage: 100000
Paul Egleston
pjmotorsports@prodigy.net
RESPONSES:
Subject: RE: 700R4, loss of line pressure
tranclin@firstworld.net
FIX:
Date: Wed Nov 15 19:35:56 PST 2000
Subject: 700R4, loss of line pressure
pjmotorsports@prodigy.net







QUESTION:
Date: Wed Oct 4 14:08:27 PDT 2000
Subject: 700R4, ATF blow out the vent
Vehicle: 1988 Chevrolet Blazer, 5.7
Mileage: 130000
Richard McClain
sprag2@aol.com
RESPONSES:
Subject: RE: 700R4, ATF blow out the vent
stardust@frontiernet.net
Subject: RE: 700R4, ATF blow out the vent
stealth@mscomm.com
FIX:
Date: Thu Nov 16 15:27:43 PST 2000
Subject: 700R4, ATF blow out the vent
sprag2@aol.com







QUESTION:
Date: Wed Nov 15 20:34:04 PST 2000
Subject: 700R4, Engine Swap
Vehicle: 1991 Chevy S-10 Blazer, 4.3
Mileage: 120,000
Gary Nelson
nelsonauto@hotmail.com
RESPONSES:
FIX:
Date: Sat Nov 18 21:16:50 PST 2000
Subject: 700R4, Engine Swap
nelsonauto@hotmail.com







QUESTION:
Date: Thu May 18 19:46:28 PDT 2000
Subject: 700R4, bind 3-4, burning coast clutches
Vehicle: 1987 chevrolet K1500 5.7l
George Whittaker
gdd2000@localaccess.com
RESPONSES;
Subject: 700R4, bind 3-4, burning coast clutches
Hi George,
I would be looking closely at the input shaft and the stator bore where it rides. Did you air check through the pump assy to see if the overrun clutches are partially applying? These like to wear the rear bushing in the stator and allow the shaft to rub. If the inner srface of the stator is worn at all replace it.
lschneg1@rochester.rr.com
Subject: 700R4, bind 3-4, burning coast clutches
I remember reading that these input shafts can twist and crack and it is hard to detect. Seems that checking involved putting it in a vise and twisting it.
marklpugliese@aol.com
Subject: 700R4, bind 3-4, burning coast clutches
What sealing rings are you using??
You should only use the solid rings for the input shaft on this transmission.
I have also traced this problem down to the tube in the stator turing and causing this problem.
Hope this helps.
roadmaster.trans@att.net
Subject: 700R4, bind 3-4, burning coast clutches
why did you use the origanal shaft? if there is a cross leak it is going to be a crack in the input shaft not the drum! this is a common problem here in the middle of texas , home of the 40ft. gooseneck tralier. most of them we see are broke in half.
batippit2@cs.com UPDATE:
Date: Fri May 19 23:18:11 PDT 2000
Subject: 700R4, bind 3-4, burning coast clutches
First, it's a 1989. Second, we checked the drum with shaft (it cross leaked), we didn't have correct shaft so we pressed it into different drum (hoping), it checked out ok so we tried it.OOPPS!!
Also, talked to customer today, a little more history, when the transmission broke after first rebuild, the converter seized up at twenty mph then released and stopped, this is quite a jolt on that imput shaft, HUH!!! Thanks again RPM!!
I really appreciate all the info on this, it's all pointing to that input. I'll let you know.
Thanks again!
gdd2000@localaccess.com MORE RESPONSES:
FIX;
Date: Fri Nov 24 22:03:43 PST 2000
QUESTION:
Date: Mon Nov 20 12:18:53 PST 2000
Subject: 700R4, Binds in Reverse
Vehicle: 1992 Chevrolet 1/2T 2wd Pick Up, 350 V-8
Mileage: 84,000
Tommy Painter
county9@yahoo.com
RESPONSES:
Subject: RE: 700R4, Binds in Reverse
claydo2@aol.com
Subject: RE: 700R4, Binds in Reverse
n8249b@chartertn.net
Subject: RE: 700R4, Binds in Reverse
rjzahn@usaor.net
Subject: RE: 700R4, Binds in Reverse
tranclin@firstworld.net
Subject: RE: 700R4, Binds in Reverse
glaenzer@csj.net
Subject: RE: 700R4, Binds in Reverse
bobauto2000@aol.com
Subject: RE: 700R4, Binds in Reverse
county9@yahoo.com
Subject: RE: 700R4, Binds in Reverse
trannydr@yellowsub.net
Subject: RE: 700R4, Binds in Reverse
inarush76@aol.com
Subject: RE: 700R4, Binds in Reverse
fwhit84684@aol.com
Subject: RE: 700R4, Binds in Reverse
info@transtechca.com
FIX:
Date: Tue Nov 28 17:13:42 PST 2000
Subject: 700R4, Binds in Reverse
county9@yahoo.com
QUESTION:
Date: Tue Oct 24 16:05:37 PDT 2000
Subject: 700R4, Flares on kickdown from 4th to 3rd
Vehicle: 1988 Chevy CK 1500 2wd, 350
Mileage: 110,000
Mark Bowler
bowler@wworld.com
RESPONSES:
Subject: RE: 700R4, Flares on kickdown from 4th to 3rd
lschneg1@rochester.rr.com
FIX:
Date: Wed Nov 29 14:49:53 PST 2000
Subject: 700R4, Flares on kickdown from 4th to 3rd
bowler@wworld.com
QUESTION:
Date: Wed Nov 29 21:09:30 PST 2000
Subject: 700R4, delay in revers . slips in reverse
Vehicle: 85 chevy camar0 z28, 5.0
Mileage: 120,000
Frank Islas
fdmaislas@aol.com
RESPONSES:
Subject: RE: 700R4, delay in revers . slips in reverse
n8249b@chartertn.net
Subject: RE: 700R4, delay in revers . slips in reverse
lindsay2@sprintmail.com
Subject: RE: 700R4, delay in revers . slips in reverse
tranclin@firstworld.net
FIX:
Date: Fri Dec 1 20:07:24 PST 2000
Subject: 700R4, delay in revers . slips in reverse
fdmaislas@aol.com
QUESTION:
Date: Tue Jun 20 15:13:00 PDT 2000
Subject: 700R4, 2/3 stack,no 3/4
Vehicle: 1990 chev pick up, 5.7 tbi
Mileage:
Kyle Tuttle
twotuts@aol.com
RESPONSES:
Subject: RE: 700R4, 2/3 stack,no 3/4
robertlb@ev1.net
Subject: RE: 700R4, 2/3 stack,no 3/4
shiftkit@specialtytrans.com
FIX:
Date: Mon Dec 11 20:38:39 PST 2000
Subject: 700R4, 2/3 stack,no 3/4
twotuts@aol.com
QUESTION:
Date: Thu Dec 21 08:54:17 PST 2000
Subject: 700R4, Installation quiery
Vehicle: 1986 Chevy K1500, 350
Mileage: 110000
Carl Wassermann
wasseca@echoincorporated.com
RESPONSES:
Subject: RE: 700R4, Installation quiery
bjr1a@mail.ru
Subject: RE: 700R4, Installation quiery
dblake@telusplanet.net
Subject: RE: 700R4, Installation quiery
yogi@mscomm.com
Subject: RE: 700R4, Installation quiery
stardust@frontiernet.net
FIX:
Date: Thu Dec 21 10:57:02 PST 2000
Subject: 700R4, Installation quiery
wasseca@echoincorporated.com
QUESTION:
Date: Tue Dec 12 15:41:46 PST 2000
Subject: 700R4, chevy drive trane
Vehicle: 85 toyota 4x4, ????
Mileage: ?????
Tony Yurkevicius
trannyman123@aol.com
RESPONSES:
Subject: RE: 700R4, chevy drive trane
dustman@wave.net
Subject: RE: 700R4, chevy drive trane
transmission_doctor@yahoo.com
Subject: RE: 700R4, chevy drive trane
tranclin@firstworld.net
FIX:
Date: Tue Dec 26 17:15:45 PST 2000
Subject: 700R4, chevy drive trane
trannyman123@aol.com
QUESTION:
Date: Fri Dec 29 03:01:29 PST 2000
Subject: 700R4, Conversion. No lockup.
Vehicle: 1991 Nissan Dual cab 4X4, 3.8ltr
Mileage: 300,000
Richard Keown
mitcham_automatics@bigpond.com
RESPONSES:
Subject: RE: 700R4, Conversion. No lockup.
woodchpr@worldnet.att.net
Subject: RE: 700R4, Conversion. No lockup.
larry_b@certifiedtrans.com
Subject: RE: 700R4, Conversion. No lockup.
county9@yahoo.com
Subject: RE: 700R4, Conversion. No lockup.
bobauto2000@aol.com
Subject: RE: 700R4, Conversion. No lockup.
dkoremus@execpc.comUPDATE:
Date: Fri Dec 29 15:08:45 PST 2000
Subject:
Richard Keown
mitcham_automatics@bigpond.com
MORE RESPONSES:
Subject: RE: 700R4, Conversion. No lockup.
cougar1972@go.com
Subject: RE: 700R4, Conversion. No lockup.
nila2@aol.com
FIX:
Date: Fri Dec 29 23:23:18 PST 2000
Subject: 700R4, Conversion. No lockup.
mitcham_automatics@bigpond.com